[Federal Register Volume 73, Number 78 (Tuesday, April 22, 2008)]
[Notices]
[Pages 21657-21668]
From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
[FR Doc No: E8-8388]
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NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from March 27, 2008, to April 9, 2008. The last
biweekly notice was published on April 8, 2008 (73 FR 19106).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice,
person(s) may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
via electronic submission through the NRC E-Filing system for a hearing
and a petition for leave to intervene. Requests for a hearing and a
petition for leave to intervene shall be filed in accordance with the
Commission's ``Rules of Practice for Domestic Licensing Proceedings''
in 10 CFR part 2. Interested person(s) should consult a current copy of
10 CFR 2.309, which is available at the Commission's PDR, located at
One White Flint North, Public File Area 01F21, 11555 Rockville Pike
(first floor), Rockville, Maryland. Publicly available records will be
accessible from the Agencywide Documents Access and Management
[[Page 21658]]
System's (ADAMS) Public Electronic Reading Room on the Internet at the
NRC Web site, http://www.nrc.gov/reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for leave to intervene is filed
within 60 days, the Commission or a presiding officer designated by the
Commission or by the Chief Administrative Judge of the Atomic Safety
and Licensing Board Panel, will rule on the request and/or petition;
and the Secretary or the Chief Administrative Judge of the Atomic
Safety and Licensing Board will issue a notice of a hearing or an
appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for hearing or a petition for leave to intervene must be
filed in accordance with the NRC E-Filing rule, which the NRC
promulgated in August 28, 2007 (72 FR 49139). The E-Filing process
requires participants to submit and serve documents over the Internet
or in some cases to mail copies on electronic storage media.
Participants may not submit paper copies of their filings unless they
seek a waiver in accordance with the procedures described below.
To comply with the procedural requirements of E-Filing, at least
five (5) days prior to the filing deadline, the petitioner/requestor
must contact the Office of the Secretary by e-mail at
[email protected], or by calling (301) 415-1677, to request (1) a
digital ID certificate, which allows the participant (or its counsel or
representative) to digitally sign documents and access the E-Submittal
server for any proceeding in which it is participating; and/or (2)
creation of an electronic docket for the proceeding (even in instances
in which the petitioner/requestor (or its counsel or representative)
already holds an NRC-issued digital ID certificate). Each petitioner/
requestor will need to download the Workplace Forms Viewer\TM\ to
access the Electronic Information Exchange (EIE), a component of the E-
Filing system. The Workplace Forms Viewer\TM\ is free and is available
at http://www.nrc.gov/site-help/e-submittals/install-viewer.html.
Information about applying for a digital ID certificate is available on
NRC's public Web site at http://www.nrc.gov/site-help/e-submittals/apply-certificates.html.
Once a petitioner/requestor has obtained a digital ID certificate,
had a docket created, and downloaded the EIE viewer, it can then submit
a request for hearing or petition for leave to intervene. Submissions
should be in Portable Document Format (PDF) in accordance with NRC
guidance available on the NRC public Web site at http://www.nrc.gov/site-help/e-submittals.html. A filing is considered complete at the
time the filer submits its documents through EIE. To be timely, an
electronic filing must be submitted to the EIE system no later than
11:59 p.m. Eastern Time on the due date. Upon receipt of a
transmission, the E-Filing system time-stamps the document and sends
the submitter an e-mail notice confirming receipt of the document. The
EIE system also distributes an e-mail notice that provides access to
the document to the NRC Office of the General Counsel and any others
who have advised the Office of the Secretary that they wish to
participate in the proceeding, so that the filer need not serve the
documents on those participants separately. Therefore, applicants and
other participants (or their counsel or representative) must apply for
and receive a digital ID certificate before a hearing request/petition
to intervene is filed so that they can obtain access to the document
via the E-Filing system.
A person filing electronically may seek assistance through the
``Contact Us'' link located on the NRC Web site at http://www.nrc.gov/site-help/e-submittals.html or by calling the NRC technical help line,
which is available between 8:30 a.m. and 4:15 p.m., Eastern Time,
Monday through Friday. The help line number is (800) 397-4209 or
locally, (301) 415-4737.
Participants who believe that they have a good cause for not
submitting documents electronically must file a motion, in accordance
with 10 CFR 2.302(g), with their initial paper filing requesting
authorization to continue to submit documents in paper format. Such
filings must be submitted by: (1) First class mail addressed to the
Office of the Secretary of the Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001, Attention: Rulemaking and
Adjudications Staff; or (2) courier, express mail, or expedited
delivery service to the Office of the Secretary, Sixteenth Floor, One
White Flint North, 11555 Rockville Pike, Rockville, Maryland 20852,
Attention:
[[Page 21659]]
Rulemaking and Adjudications Staff. Participants filing a document in
this manner are responsible for serving the document on all other
participants. Filing is considered complete by first-class mail as of
the time of deposit in the mail, or by courier, express mail, or
expedited delivery service upon depositing the document with the
provider of the service.
Non-timely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission, the presiding
officer, or the Atomic Safety and Licensing Board that the petition
and/or request should be granted and/or the contentions should be
admitted, based on a balancing of the factors specified in 10 CFR
2.309(c)(1)(i)-(viii). To be timely, filings must be submitted no later
than 11:59 p.m. Eastern Time on the due date.
Documents submitted in adjudicatory proceedings will appear in
NRC's electronic hearing docket which is available to the public at
http://ehd.nrc.gov/EHD_Proceeding/home.asp, unless excluded pursuant
to an order of the Commission, an Atomic Safety and Licensing Board, or
a Presiding Officer. Participants are requested not to include personal
privacy information, such as social security numbers, home addresses,
or home phone numbers in their filings. With respect to copyrighted
works, except for limited excerpts that serve the purpose of the
adjudicatory filings and would constitute a Fair Use application,
participants are requested not to include copyrighted materials in
their submission.
For further details with respect to this amendment action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, http://www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to [email protected].
Entergy Nuclear Vermont Yankee, LLC and Entergy Nuclear Operations,
Inc., Docket No. 50-271, Vermont Yankee Nuclear Power Station, Vernon,
Vermont
Date of amendment request: February 12, 2008.
Description of amendment request: The proposed amendment would
revise the Technical Specification (TS) Sections 2.1, ``Limiting Safety
System Setting,'' 3.1, ``Reactor Protection System,'' 3.2, ``Protective
Instrument Systems,'' associated Surveillance Requirements, and other
TS with similar requirements as these instrumentation TS sections.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The operation of Vermont Yankee Nuclear Power Station in
accordance with the proposed amendment will not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
The proposed changes do not significantly affect the design or
fundamental operation and maintenance of the plant. Accident
initiators or the frequency of analyzed accident events are not
significantly affected as a result of the proposed changes;
therefore, there will be no significant change to the probabilities
of accidents previously evaluated.
The proposed changes do not significantly alter assumptions or
initial conditions relative to the mitigation of an accident
previously evaluated. The proposed changes continue to ensure
process variables, structures, systems, and components (SSCs) are
maintained consistent with the safety analyses and licensing basis.
The revised technical specifications continue to require that SSCs
are properly maintained to ensure operability and performance of
safety functions as assumed in the safety analyses. Since the design
basis events analyzed in the safety analyses will not change
significantly, the consequences of these events will not change as a
result of the proposed changes to the TS.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The operation of Vermont Yankee Nuclear Power Station in
accordance with the proposed amendment will not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
The proposed changes do not involve any physical alteration of
the plant (no new or different types of equipment being installed)
and do not involve a change in the design, normal configuration or
basic operation of the plant. The proposed changes do not introduce
any new accident initiators. In some cases, the proposed changes
impose different or more restrictive requirements; however, these
new requirements are consistent with the assumptions in the safety
analyses and current licensing basis. Where requirements are
relocated to other licensee-controlled documents, adequate controls
exist to ensure proper maintenance of the requirements and continued
operability of the associated equipment.
The proposed changes do not involve significant changes in the
fundamental methods governing normal plant operations and do not
require unusual or uncommon operator actions. The proposed changes
provide assurance that the plant will not be operated in a mode or
condition that violates the essential assumptions or initial
conditions in the safety analyses and that SSCs remain capable of
performing the intended safety functions as assumed in the same
analyses. Consequently, the response of the plant and the plant
operator to postulated events will not be significantly different.
Therefore, the proposed TS change does not create the
possibility of a new or different kind of accident from any
previously evaluated.
3. The operation of Vermont Yankee Nuclear Power Station in
accordance with the proposed amendment will not involve a
significant reduction in a margin of safety.
Margin of safety is related to the confidence in the ability of
the fission product barriers to perform their design functions
during and following an accident situation. The proposed changes do
not significantly affect any of the assumptions, initial conditions
or inputs to the safety analyses. Plant design is unaffected by
these proposed changes and will continue to provide adequate
defense-in-depth and diversity of safety functions as assumed in the
safety analyses; therefore no significant reduction in the margin of
safety will result.
There are no proposed changes to the Safety Limits and only
administrative and one more restrictive change to Limiting System
Setting requirements. The proposed changes maintain requirements
consistent with safety analyses assumptions and the licensing basis.
Fission product barriers will continue to meet their design
capabilities without any significant impact to their ability to
maintain parameters within acceptable limits. The safety functions
are maintained within acceptable limits without any significant
decrease in capability.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. William C. Dennis, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 400 Hamilton Avenue, White
Plains, NY 10601.
NRC Branch Chief: Mark G. Kowal.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit No. 1, Lake County, Ohio
Date of amendment request: February 20, 2008.
Description of amendment request: The amendment request would
revise
[[Page 21660]]
the technical specifications (TSs) to adopt NRC-approved Revision 1 to
TS Task Force (TSTF) Standard Technical Specification Change Traveler
TSTF-476, ``Improved Banked Position Withdrawal Sequence (BPWS) Control
Rod Insertion Process (NEDO-33091).'' The amendment would revise an
applicability footnote in the TS Table 3.3.2.1-1, ``Control Rod Block
Instrumentation,'' to permit use of an improved, optional BPWS reactor
shutdown process. Corresponding changes are made to the Bases of TS
3.1.6, ``Control Rod Pattern,'' and the Bases of TS 3.3.2.1, to
reference the new BPWS shutdown method.
The NRC staff issued a notice of opportunity for comment in the
Federal Register on May 3, 2006 (71 FR 26118), on possible license
amendments adopting TSTF-476 using the NRC's consolidated line item
improvement process for amending licensee's TSs, which included a model
safety evaluation (SE) and a model no significant hazards consideration
(NSHC) determination. The NRC staff subsequently issued a notice of
availability of the models for referencing in license amendment
applications in the Federal Register on May 23, 2007 (72 FR 29004-
29010), which included the resolution of public comments on the model
SE. The May 23, 2007, notice of availability referenced the May 3,
2006, notice. The licensee has affirmed the applicability of the
following NSHC determination in its application.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed changes modify the TS to allow the use of the improved
banked position withdrawal sequence (BPWS) during shutdowns if the
conditions of NEDO-33091-A, Revision 2, ``Improved BPWS Control Rod
Insertion Process,'' July 2004, have been satisfied. The staff finds
that the licensee's justifications to support the specific TS changes
are consistent with the approved topical report and TSTF-476, Revision
1. Since the change only involves changes in control rod sequencing,
the probability of an accident previously evaluated is not
significantly increased, if at all. The consequences of an accident
after adopting TSTF-476 are no different than the consequences of an
accident prior to adopting TSTF-476. Therefore, the consequences of an
accident previously evaluated are not significantly affected by this
change. Therefore, this change does not involve a significant increase
in the probability or consequences of an accident previously evaluated.
Criterion 2--The Proposed Change Does Not Create the Possibility of a
New or Different Kind of Accident From any Previously Evaluated
The proposed change will not introduce new failure modes or effects
and will not, in the absence of other unrelated failures, lead to an
accident whose consequences exceed the consequences of accidents
previously evaluated. The control rod drop accident (CRDA) is the
design basis accident for the subject TS changes. This change does not
create the possibility of a new or different kind of accident from an
accident previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The proposed change, TSTF-476, Revision 1, incorporates the
improved BPWS, previously approved in NEDO-33091-A, into the improved
TS. The control rod drop accident (CRDA) is the design basis accident
for the subject TS changes. In order to minimize the impact of a CRDA,
the BPWS process was developed to minimize control rod reactivity worth
for BWR plants. The proposed improved BPWS further simplifies the
control rod insertion process, and in order to evaluate it, the staff
followed the guidelines of Standard Review Plan Section 15.4.9, and
referred to General Design Criterion 28 of Appendix A to 10 CFR part 50
as its regulatory requirement. The TSTF stated the improved BPWS
provides the following benefits: (1) Allows the plant to reach the all-
rods-in condition prior to significant reactor cool down, which reduces
the potential for re-criticality as the reactor cools down; (2) reduces
the potential for an operator reactivity control error by reducing the
total number of control rod manipulations; (3) minimizes the need for
manual scrams during plant shutdowns, resulting in less wear on control
rod drive (CRD) system components and CRD mechanisms; and (4)
eliminates unnecessary control rod manipulations at low power,
resulting in less wear on reactor manual control and CRD system
components. The addition of procedural requirements and verifications
specified in NEDO-33091-A, along with the proper use of the BPWS will
prevent a control rod drop accident (CRDA) from occurring while power
is below the low power setpoint (LPSP). The net change to the margin of
safety is insignificant. Therefore, this change does not involve a
significant reduction in a margin of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, Mail Stop A-GO-15, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Russell Gibbs.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: March 24, 2008.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) Section 3.7.3, ``Reactor Equipment
Cooling (REC) System,'' to allow credit for the ability to align the
service water (SW) system to the REC system.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
Four design basis accidents have been previously evaluated at
CNS [Cooper Nuclear Station]. These are (1) a control rod drop
accident, in which a control rod inserted into the reactor core
becomes uncoupled and drops out of the reactor core during
operation; (2) a loss-of-coolant accident [LOCA], in which a pipe in
the reactor coolant system breaks, resulting in a loss of reactor
coolant inventory and the ability to cool the nuclear fuel; (3) a
fuel handling accident, in which a fuel assembly is dropped during
fuel handling operations and impacts fuel assemblies in the reactor
core; and (4) a main steam line break accident, in which a main
steam line breaks resulting in the discharge of steam at high
pressure and temperature.
The proposed license amendment makes no changes to the design or
operation of the control rod drive system. Thus, there is no
increase in the probability of a control rod drop accident.
The proposed license amendment makes no changes to the design or
operation of the reactor coolant system. Thus, there is no increase
in the probability of a loss-of-coolant accident. (The design basis
LOCA does not involve a postulated break in the systems associated
with the proposed license amendment).
The proposed license amendment makes no changes to the design of
the fuel handling
[[Page 21661]]
system, or to the method of moving fuel. Thus, there is no increase
in the probability of a fuel handling accident.
The proposed license amendment makes no changes to the design of
the main steam system or to how the reactor is operated. Thus, there
is no increase in the probability of a main steam line break
accident.
Based on the above, the proposed changes do not result in a
significant increase in the probability of an accident previously
evaluated.
The SW System is able to supply sufficient cooling to perform
the function of the REC System to remove the heat generated by the
ECCS [emergency core cooling system] pumps, as well as providing
sufficient cooling to the heat loads in the SW System. Aligning the
SW System to the REC System sooner than the current seven days, as
will be allowed by the proposed changes to the TS, will not
adversely impact the ability of the ECCS pumps to meet their
function.
Because the function of the REC System is to remove the heat
generated by the ECCS pumps from the rooms in which the pumps are
located, the REC system is indirectly involved in the mitigation of
an accident.
Based on the above, the change does not involve a significant
increase in the consequences of an accident previously evaluated.
NPPD [Nebraska Public Power District] concludes that the
proposed changes do not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed license amendment would allow continued plant
operation with leakage from the REC System in excess of limits,
provided that the required cooling water can be supplied by the SW
System. This involves revising the actions for mitigating a LOCA, in
that the SW System may need to be aligned to the REC System sooner
than 7 days following a LOCA, as is required by the current
licensing basis. Allowing leakage from the REC System to exceed
limits and requiring that the SW System be aligned to the REC System
sooner than what is currently required by the licensing basis does
not create the possibility of a new or different kind of accident
from any previously evaluated.
The proposed license amendment request does not involve physical
modification of any system in the plant, nor do they involve a
change to how the plant is operated. No new equipment is being
added. Use of the SW System to supply water to the REC System in the
event of REC leakage is part of the current CNS design and licensing
basis.
Based on the above NPPD concludes that these proposed changes do
not create the possibility of a new or different kind of accident
from any previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
This proposed license amendment would revise TS to allow
continued plant operation with leakage from the REC System in excess
of limits, provided that the SW System can be aligned to the REC
System and supply the cooling water required by the REC System to
meet its safety function. The safety function of the REC System is
to remove the heat generated by the ECCS pumps from the rooms in
which the pumps are located. This proposed change to TS revises the
timing for taking an action involved in mitigating a LOCA, in that
the SW System may need to be aligned to the REC System sooner than
seven days following a LOCA, as currently allowed by license
requirements. It has been demonstrated that this alignment can be
made sooner than the current required seven days. Making this
alignment sooner than seven days does not adversely impact the
ability to mitigate a LOCA.
Based on the above, NPPD concludes that these proposed changes
do not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Branch Chief: Thomas G. Hiltz.
Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339,
North Anna Power Station, Units No. 1 and No. 2, Louisa County,
Virginia
Date of amendment request: March 19, 2008.
Description of amendment request: The proposed amendment would
delete the main control room/emergency switchgear room (MCR/ESGR)
bottled air system from Technical Specifications. Operation of the
bottled air system will be controlled by the Updated Final Safety
Analysis Report.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed license amendment involve a significant
increase in the probability or consequences of an accident
previously evaluated?
The proposed changes do not adversely affect accident initiators
or precursors nor alter the design assumptions of the facility. The
proposed changes do not alter or prevent the ability of structures,
systems, and components (SSCs) from performing their required safety
function of mitigating the consequences of an initiating event
within the established acceptance limits. The proposed changes to
the MCR/ESGR Bottled Air System and Emergency Ventilation System
[EVS] do not affect the probability of an accident previously
evaluated because the subject SSCs are not an initiator or precursor
to any accident previously evaluated. The Technical Specifications
changes noted above will ensure the SSCs are operable to mitigate
the consequences of an accident.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed license amendment create the possibility of
a new or different kind of accident from any accident previously
evaluated?
Deletion of the MCR/ESGR Bottled Air System does not create the
possibility of a new or different kind of accident. The other
proposed changes do not alter the operability requirements of the
MCR/ESGR emergency ventilation system or MCR/ESGR isolation.
Therefore, the control room habitability systems remain operable to
mitigate the consequences of a [design-basis accident] DBA. The
changes do not involve a physical alteration of the plant systems
credited in the accident analysis (i.e., no new or different type of
equipment will be installed) or a significant change in the methods
governing normal plant operation. The MCR/ESGR EVS is maintained in
a standby mode and its operation does not generate any new accidents
or accident precursors.
Therefore, this change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
The proposed changes do not alter the manner in which safety
limits, limiting safety system settings, or limiting conditions for
operation are determined. The current dose analysis acceptance
criteria are not affected by these changes. The proposed changes
will not result in plant operation in a configuration outside the
analyses or design basis. The proposed changes do not adversely
affect systems that are required to respond for safe shutdown of the
plant and to maintain the plant in a safe operating condition.
Therefore, this change does not involve a significant reduction in
a margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on this review, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Esq., Senior Counsel,
Dominion Resources Services, Inc., Millstone Power Station, Building
475, 5th Floor, Rope Ferry Road, Rt. 156, Waterford, Connecticut 06385.
NRC Branch Chief: Melanie C. Wong.
[[Page 21662]]
Previously Published Notices of Consideration of Issuance of Amendments
to Facility Operating Licenses, Proposed No Significant Hazards
Consideration Determination, and Opportunity for a Hearing
The following notices were previously published as separate
individual notices. The notice content was the same as above. They were
published as individual notices either because time did not allow the
Commission to wait for this biweekly notice or because the action
involved exigent circumstances. They are repeated here because the
biweekly notice lists all amendments issued or proposed to be issued
involving no significant hazards consideration.
For details, see the individual notice in the Federal Register on
the day and page cited. This notice does not extend the notice period
of the original notice.
Duke Power Company LLC, Docket Nos. 50-413 and 50-414, Catawba Nuclear
Station, Units 1 and 2, York County, South Carolina
Duke Power Company LLC, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment request: February 15, 2008.
Brief description of amendment request: The amendments authorized a
change to the UFSAR requiring an inspection of each ice condenser
within 24 hours of experiencing a seismic event greater than or equal
to an operating basis earthquake within the five (5) week period after
ice basket replenishment has been completed to confirm that adverse ice
fallout has not occurred which could impede the ability of the ice
condenser lower inlet doors to open. This action would be taken, in
lieu of requiring a five week waiting period following ice basket
replenishment, prior to beginning ascension to power operations.
Date of publication of individual notice in Federal Register:
February 26, 2008 (73 FR 10302).
Expiration date of individual notice: April 28, 2008.
Notice of Issuance of Amendments to Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR chapter I, which are set
forth in the license amendment.
Notice of Consideration of Issuance of Amendment to Facility
Operating License, Proposed No Significant Hazards Consideration
Determination, and Opportunity for A Hearing in connection with these
actions was published in the Federal Register as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.22(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items are available for public inspection at
the Commission's Public Document Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555 Rockville Pike (first floor),
Rockville, Maryland. Publicly available records will be accessible from
the Agencywide Documents Access and Management Systems (ADAMS) Public
Electronic Reading Room on the Internet at the NRC Web site, http://www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to [email protected].
Dominion Energy Kewaunee, Inc. Docket No. 50-305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of application for amendment: June 12, 2007, as supplemented
on December 12, 2007.
Brief description of amendment: The amendment revised the P-7 and
P-10 nuclear instrumentation system permissive setpoints in Technical
Specification (TS) Table 3.5-2, ``Instrument Operation Conditions for
Reactor Trip,'' revised the Table format and added a footnote
explaining that the turbine impulse pressure setting limit is converted
to an equivalent turbine impulse pressure, and revised TS 2.3,
``Instrumentation System,'' concerning reactor trip interlocks to be
consistent with the proposed changes to TS Table 3.5-2.
Date of issuance: March 28, 2008.
Effective date: As of the date of issuance and shall be implemented
within 60 days.
Amendment No.: 195.
Facility Operating License No. DPR-43: Amendment revised the
License and Technical Specifications.
Date of initial notice in Federal Register: August 28, 2007 (72 FR
49570)
The December 12, 2007, letter provided clarifying information that
did not change the scope of the proposed amendment as described in the
original notice of proposed action published in the Federal Register
(72 FR 49570) and did not change the initial proposed no significant
hazards determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 28, 2008.
No significant hazards consideration comments received: No.
Dominion Energy Kewaunee, Inc. Docket No. 50-305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of application for amendment: September 24, 2007, as
supplemented on January 18, 2008.
Brief description of amendment: The amendment revises the Technical
Specifications (TSs) to add a reference to Dominion Topical Report DOM-
NAF-5, ``Application of Dominion Nuclear Core Design and Safety
Analysis Methods to the Kewaunee Power Station (KPS),'' to the list of
approved analytical methods. The amendment permits the application of
the Dominion nuclear core design and safety analysis methods, including
the methodology to perform core thermal-hydraulic analysis to predict
critical heat flux and departure from nucleate boiling ratio for the
Westinghouse 422 V+ fuel design. In addition, the amendment: (1)
Accommodates the use of the methodologies in DOM-NAF-5; (2) deletes one
approved analytical method that will no longer be used; and (3) deletes
date and revision numbers from the current TS list of approved
analytical methods, consistent with TS Task Force (TSTF) Change
Traveler TSTF-363-A, Revision 0, ``Revise Topical Report References in
ITS [improved TSs] 5.6.5, COLR [Core Operating Limits Report],'' dated
August 4, 2003, and adds a TS that requires complete identification of
those analytical methods in the COLR.
Date of issuance: March 28, 2008.
[[Page 21663]]
Effective date: As of the date of issuance and shall be implemented
within 60 days.
Amendment No.: 196.
Facility Operating License No. DPR-43: Amendment revised the
Technical Specifications and the License.
Date of initial notice in Federal Register: October 23, 2007 (72 FR
60034). The January 18, 2008, supplement provided additional
information that clarified the application, did not expand the scope of
the application as originally noticed, and did not change the staff's
original proposed no significant hazards consideration determination as
published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 28, 2008.
No significant hazards consideration comments received: No.
Dominion Energy Kewaunee, Inc. Docket No. 50-305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of application for amendment: March 17, 2006, as supplemented
on April 17 and September 17, 2007, and February 1 and March 10, 2008.
Brief description of amendment: The amendment revised Appendix B,
``Special Design Procedures,'' of the Updated Safety Analysis Report
(USAR) to modify the design criteria for internal flooding evaluations.
The revisions included modifications to Section B.5, ``Protection of
Class I Items,'' and Section B.11, ``Internal Flooding.''
Date of issuance: March 28, 2008.
Effective date: As of the date of issuance and will be implemented
by incorporating the revisions into the next update of the USAR, as
required by 10 CFR 50.71(c).
Amendment No.: 197.
Facility Operating License No. DPR-43: Amendment revised the USAR
and License.
Date of initial notice in Federal Register: April 25, 2006 (71 FR
23954). The letters dated April 17 and September 17, 2007, and February
1 and March 10, 2008, provided clarifying information that did not
change the scope of the proposed amendment as described in the original
notice of proposed action published in the Federal Register and did not
change the initial proposed no significant hazards determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 28, 2008.
No significant hazards consideration comments received: No.
Dominion Nuclear Connecticut, Inc., Docket No. 50-336, Millstone Power
Station, Unit No. 2, New London County, Connecticut
Date of application for amendment: March 28, 2007, as supplemented
by letter dated March 10, 2008.
Brief description of amendment: The amendment modifies the
Technical Specification Surveillance Requirement 4.6.2.1.1.e to allow
performance of testing for nozzle blockage to be based on the
occurrence of activities that could potentially result in nozzle
blockage rather than a fixed periodic basis.
Date of issuance: March 31, 2008.
Effective date: As of the date of issuance and shall be implemented
within 60 days from the date of issuance.
Amendment No.: 303.
Renewed Facility Operating License No. DPR-65: Amendment revised
the License and Technical Specifications.
Date of initial notice in Federal Register: January 15, 2008 (73 FR
2549). The March 10, 2008, supplement, contained clarifying information
and did not change the NRC staff's initial proposed finding of no
significant hazards consideration.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 31, 2008.
No significant hazards consideration comments received: No.
Duke Energy Carolinas, LLC Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of application for amendments: February 15, 2008.
Brief description of amendments: The amendments would authorize a
change to the Updated Final Safety Analysis Report (UFSAR) requiring an
inspection of each ice condenser unit within 24 hours of experiencing a
seismic event greater than or equal to an operating basis earthquake
within the 5-week period after ice basket replenishment has been
completed to confirm that adverse ice fallout has not occurred which
could impede the ability of the ice condenser lower inlet doors to
open. This action would be taken, in lieu of requiring a 5-week waiting
period following ice basket replenishment, prior to beginning ascension
to power operations.
Date of issuance: April 2, 2008.
Effective date: As of the date of issuance and shall be implemented
within 30 days from the date of issuance.
Amendment Nos.: 246, 226.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the licenses.
Date of initial notice in Federal Register: February 26, 2008 (73
FR 10302). The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated April 2, 2008.
No significant hazards consideration comments received: No.
Duke Power Company LLC, et al., Docket Nos. 50-413 and 50-414, Catawba
Nuclear Station, Units 1 and 2, York County, South Carolina
Duke Power Company LLC, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Duke Power Company LLC, Docket Nos. 50-269, 50-270, and 50-287, Oconee
Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
Oconee Nuclear Station Independent Spent Fuel Storage Installation
License No. SNM-2503, Docket No. 72-4, Oconee County, South Carolina
Date of application for amendments: March 14, 2007.
Brief description of amendments: The amendments would revise the
licenses to reflect the change in the name of the licensee from Duke
Power Company LLC to Duke Energy Carolinas, LLC. The proposed
amendments are a name change only. There is no change in the state of
incorporation, registered agent, registered office, rights, or
liabilities of the company. Nor is there a change in the function of
the licensee or the way in which it does business.
Date of issuance: March 28, 2008.
Effective date: As of the date of issuance and shall be implemented
within 30 days from the date of issuance.
Amendment Nos.: 240, 234.
Renewed Facility Operating License Nos. NPF-35 and NPF-52:
Amendments revised the licenses.
Amendment Nos.: 245, 225.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the licenses.
Amendment Nos.: 361, 363, 362.
Renewed Facility Operating License Nos. DPR-38, DPR-47, and DPR-55:
Amendments revised the licenses.
Amendment No.: 9.
Independent Spent Fuel Storage Installation License No. SNM-2503:
Amendment revised the license.
Date of initial notice in Federal Register: December 4, 2007 (72 FR
68210).
[[Page 21664]]
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated March 28, 2008.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
No. 2, Pope County, Arkansas
Date of application for amendment: July 31, 2007, as supplemented
by letters dated July 31, 2007, and March 11, 2008.
Brief description of amendment: The proposed changes revised
Technical Specification 6.6.5, ``Core Operating Limits Report (COLR),''
which would add new analytical methods to support the implementation of
Next Generation Fuel.
Date of issuance: March 26, 2008.
Effective date: As of the date of issuance and shall be implemented
prior to startup following the spring 2008 refueling outage.
Amendment No.: 276.
Renewed Facility Operating License No. NPF-6: Amendment revised the
Technical Specifications, Facility Operating License, and the Final
Safety Analysis Report.
Date of initial notice in Federal Register: August 28, 2007 (72 FR
49576). The supplemental letters dated July 31, 2007, and March 11,
2008, provided additional information that clarified the application,
did not expand the scope of the application as originally noticed, and
did not change the staff's original proposed no significant hazards
consideration determination as published in the Federal Register The
Commission's related evaluation of the amendment is contained in a
Safety Evaluation dated March 26, 2008.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
No. 2, Pope County, Arkansas
Date of application for amendment: April 24, 2007.
Brief description of amendment: The amendment revised Technical
Specification (TS) 5.2.1, ``Fuel Assemblies,'' to add Optimized
ZIRLOTM as an acceptable fuel rod cladding material.
Date of issuance: March 26, 2008.
Effective date: As of the date of issuance and shall be implemented
within 60 days from the date of issuance.
Amendment No.: 277.
Renewed Facility Operating License No. NPF-6: Amendment revised the
Technical Specifications/license.
Date of initial notice in Federal Register: June 5, 2007 (72 FR
31099). The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated March 26, 2008.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
No. 2, Pope County, Arkansas
Date of application for amendment: October 5, 2007, as supplemented
by letter dated February 19, 2008.
Brief description of amendment: The amendment revised the Technical
Specifications (TS) 3.6.2.2, ``Containment Sump Buffering Agent
Trisodium Phosphate (TSP)'' and its associated Surveillance Requirement
4.6.2.2 to replace references to TSP with the sodium tetraborate (NaTB)
buffering agent. The required volume of NaTB has also been changed to
reflect the new buffer. In addition, the title has been changed to
remove the reference to TSP.
Date of issuance: March 31, 2008.
Effective date: As of the date of issuance and shall be implemented
following completion of the 2R19 refueling outage in spring 2008.
Amendment No.: 278.
Renewed Facility Operating License No. NPF-6: Amendment revised the
Technical Specifications/license.
Date of initial notice in Federal Register: November 6, 2007 (72 FR
62688). The supplemental letter dated February 19, 2008, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the staff's original proposed no significant hazards consideration
determination as published in the Federal Register. The Commission's
related evaluation of the amendment is contained in a Safety Evaluation
dated March 31, 2008.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit
No. 1, Pope County, Arkansas
Date of amendment request: October 22, 2007.
Brief description of amendment: The amendment revised Technical
Specification (TS) Limiting Condition for Operation (LCO) 3.0.4 and
Surveillance Requirement 4.0.4 to adopt the provisions of Industry/TS
Task Force (TSTF) change TSTF-359, ``Increased Flexibility in Mode
Restraints.'' This operating license improvement was made available by
the U.S. Nuclear Regulatory Commission on April 4, 2003, as part of the
consolidated line item improvement process.
Date of issuance: April 2, 2008.
Effective date: As of the date of issuance and shall be implemented
within 60 days from the date of issuance.
Amendment No.: Unit 1--232.
Renewed Facility Operating License No. DPR-51: Amendment revised
the Technical Specifications/license.
Date of initial notice in Federal Register: December 18, 2007 (72
FR 71709). The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated April 2, 2008.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
No. 2, Pope County, Arkansas
Date of application for amendment: May 8, 2007, as supplemented by
letter dated March 28, 2008.
Brief description of amendment: The amendment modified the Arkansas
Nuclear One, Unit 2, Technical Specification 3.1.1.4, ``Moderator
Temperature Coefficient (MTC).'' Specifically, the change modified the
surveillance frequency to be based on effective full power days instead
of boron concentration.
Date of issuance: March 31, 2008.
Effective date: As of the date of issuance and shall be implemented
within 60 days from the date of issuance.
Amendment No.: 279.
Renewed Facility Operating License No. NPF-6: Amendment revised the
Technical Specifications/license.
Date of initial notice in Federal Register: June 5, 2007 (72 FR
31099). The supplemental letter dated March 28, 2008, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the staff's original proposed no significant hazards consideration
determination as published in the Federal Register. The Commission's
related evaluation of the amendment is contained in a Safety Evaluation
dated March 31, 2008.
No significant hazards consideration comments received: No.
Exelon Generation Company, LLC, Docket Nos. STN 50-456 and STN 50-457,
Braidwood Station (Braidwood), Units 1 and 2, Will County, Illinois
Date of application for amendment: April 4, 2007, as supplemented
by letters dated October 10, 2007, January 31, and February 26, 2008.
Brief description of amendment: The amendments revise Technical
[[Page 21665]]
Specification 5.5.16, ``Containment Leakage Rate Testing Program,'' to
reflect a one-time, 5-year extension of the current containment Type A
test (containment integrated leakage rate test (ILRT)) interval
requirement, under Title 10 of the Code of Federal Regulations, Part
50, Appendix J, Option B, from 10 years to 15 years. The amendments
allow the next Type A ILRT to be performed within 15 years of the most
recent Type A test at Braidwood, but no later than October 5, 2013, for
Unit 1, and no later than May 4, 2014, for Unit 2.
Date of issuance: April 2, 2008.
Effective date: As of the date of issuance and shall be implemented
within 30 days.
Amendment Nos.: Unit 1-149; Unit 2-149.
Facility Operating License Nos. NPF-72 and NPF-77: The amendment
revised the Technical Specifications and License.
Date of initial notice in Federal Register: June 5, 2007 (72 FR
31100). The October 10, 2007, January 31, and February 26, 2008,
supplemental letters contained clarifying information and did not
change the NRC staff's original proposed no significant hazards
consideration. The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated April 2, 2008.
No significant hazards consideration comments received: No.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-412,
Beaver Valley Power Station, Unit No. 2, Beaver County, Pennsylvania.
Date of application for amendment: June 14, 2006, as supplemented
by letters dated July 20, July 26, December 21, 2007, and March 11,
2008.
Brief description of amendment: The amendment will revise Technical
Specifications (TSs) to incorporate the results of a new spent fuel
pool (SFP) criticality analysis documented in WCAP-16518-P, ``Beaver
Valley Unit 2 Spent Fuel Pool Criticality Analysis,'' Revision 2 for
BVPS-2. The new criticality analysis will permit utilization of vacant
storage locations dictated by the existing TS storage configurations in
the BVPS-2 SFP.
Date of issuance: March 27, 2008.
Effective date: As of the date of issuance, and shall be
implemented within 30 days.
Effective date: As of the date of issuance, and shall be
implemented within 30 days.
Amendment No: 165.
Facility Operating License No. NPF-73. Amendment revised the
License and TS.
Date of initial notice in Federal Register: August 15, 2006 (71 FR
46935). The supplements dated July 20, July 26, December 21, 2007, and
March 11, 2008, provided additional information that clarified the
application, did not expand the scope of the application as originally
noticed, and did not change the Nuclear Regulatory Commission (NRC)
staff(s original proposed no significant hazards consideration
determination as published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 27, 2008.
No significant hazards consideration comments received: No.
FPL Energy Seabrook, LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: March 29, 2007, as supplemented by
letter dated January 9, 2008.
Description of amendment request: The amendment revises the
Seabrook Station, Unit No 1, Technical Specifications to increase the
power level required for a reactor trip following a turbine trip (P-9
setpoint).
Date of issuance: March 27, 2008.
Effective date: As of its date of issuance, and shall be
implemented within 90 days.
Amendment No.: 117.
Facility Operating License No. NPF-86: The amendment revised the
License and Technical Specifications.
Date of initial notice in Federal Register: July 31, 2007 (72 FR
41785). The licensee's January 9, 2008, supplement provided clarifying
information that did not change the scope of the proposed amendment as
described in the original notice of proposed action published in the
Federal Register, and did not change the initial proposed no
significant hazards consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated March 27, 2008.
No significant hazards consideration comments received: No.
Luminant Generation Company LLC, Docket Nos. 50-445 and 50-446,
Comanche Peak Steam Electric Station, Unit Nos. 1 and 2, Somervell
County, Texas
Date of amendment request: April 10, 2007, as supplemented by
letters dated July 31, August 16, November 15 (two letters), and
November 19, 2007, and February 11, March 6, March 13, and March 26,
2008.
Brief description of amendments: The amendments revised Technical
Specification (TS) 3.1, ``Reactivity Control Systems,'' TS 3.2, ``Power
Distribution Limits,'' TS 3.3, ``Instrumentation,'' and TS 5.6.5b,
``Core Operating Limits Report (COLR),'' to incorporate standard
Westinghouse-developed and NRC-approved analytical methods into the
list of methodologies used to establish the core operating limits.
Date of issuance: April 2, 2008.
Effective date: As of the date of issuance and shall be implemented
prior to startup from refueling outage 10 for Comanche Peak Steam
Electric Station, Unit 2.
Amendment Nos.: Unit 1--144; Unit 2--144.
Facility Operating License Nos. NPF-87 and NPF-89: The amendments
revised the Facility Operating Licenses and Technical Specifications.
Date of initial notice in Federal Register: August 14, 2007 (72 FR
45461). The supplemental letters dated July 31, August 16, November 15
(two letters), and November 19, 2007, and February 11, March 6, March
13, and March 26, 2008, provided additional information that clarified
the application, did not expand the scope of the application as
originally noticed, and did not change the staff's original proposed no
significant hazards consideration determination as published in the
Federal Register on August 14, 2007 (72 FR 45461). The Commission's
related evaluation of the amendments is contained in a Safety
Evaluation dated April 2, 2008.
No significant hazards consideration comments received: No.
Luminant Generation Company LLC, Docket Nos. 50-445 and 50-446,
Comanche Peak Steam Electric Station, Unit Nos. 1 and 2, Somervell
County, Texas
Date of amendment request: August 16, 2007, as supplemented by
letter dated December 13, 2007.
Brief description of amendments: The amendments revised Technical
Specification (TS) 3.1.4, ``Rod Group Alignment Limits,'' Table 3.3.1-
1, ``Reactor Trip System Instrumentation,'' Table 3.3.2-1, ``Engineered
Safety Feature Actuation System Instrumentation,'' TS 3.4.10,
``Pressurizer Safety Valves,'' TS 3.7.1, ``Main Steam Safety Valves
(MSSVs),'' and Table 3.7.1-1, ``Operable Main Steam Safety Valves
Versus Maximum Allowable Power.'' The change to the TS is to reflect
cycle-specific safety analysis assumptions and the results associated
with the adoption of
[[Page 21666]]
Westinghouse accident analyses methodologies.
Date of issuance: April 3, 2008.
Effective date: As of the date of issuance and shall be implemented
prior to startup from the fall 2008 refueling outage for Unit 1, and
prior to startup from the spring 2008 refueling outage for Unit 2.
Amendment Nos.: Unit 1--145; Unit 2--145.
Facility Operating License Nos. NPF-87 and NPF-89: The amendments
revised the Facility Operating Licenses and Technical Specifications.
Date of initial notice in Federal Register: September 25, 2007 (72
FR 54482). The supplemental letter dated December 13, 2007, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the staff's original proposed no significant hazards consideration
determination as published in the Federal Register on September 25,
2007 (72 FR 54482). The Commission's related evaluation of the
amendments is contained in a Safety Evaluation dated April 3, 2008
No significant hazards consideration comments received: No.
National Aeronautics and Space Administration, Docket Nos. 50-30 and
50-185, Plum Brook Reactor Facility, Sandusky, Ohio (TAC NOS. J60622
and J60626)
Date of application for amendments: February 9, 2007.
Brief description of amendments: The amendments to facility
licenses include revisions to the Technical Specifications, and
incorporates Final Status Survey Plan (Revision 1). The same Technical
Specifications apply equally to both licenses.
Date of issuance: March 24, 2008.
Effective date: As of the date of issuance.
Amendment Nos.: 13 and 9.
Facility License Nos. TR-3 and R-93: The amendments revise the
facility licenses.
Date of initial notice in Federal Register: August 20, 2007 (72 FR
46521).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation enclosed with the amendment dated March 24,
2008.
No significant hazards consideration comments received: No.
Nine Mile Point Nuclear Station, LLC, Docket No. 50-410, Nine Mile
Point Nuclear Station, Unit No. 2 (NMP2), Oswego County, New York
Date of application for amendment: October 22, 2007.
Brief description of amendment: The amendment revises the NMP2
Technical Specifications (TSs) by deleting the requirements related to
the hydrogen recombiners and hydrogen and oxygen monitors. A notice of
availability for this TS improvement using the consolidated line item
improvement process was published in the Federal Register on September
25, 2003 (68 FR 55416). In addition, the amendment revises Operating
License No. NPF-69 by deleting paragraph 2.C.(11a) from the operating
license, and retaining the current licensing basis hydrogen monitoring
requirements in the NMP2 Updated Final Safety Analysis Report.
Date of issuance: April 8, 2008.
Effective date: As of the date of issuance to be implemented within
60 days.
Amendment No.: 124.
Renewed Facility Operating License No. NPF-69: Amendment revises
the License and Technical Specifications.
Date of initial notice in Federal Register: December 4, 2007 (72 FR
68217). The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated April 8, 2008.
No significant hazards consideration comments received: No.
Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station,
Unit No. 1, Washington County, Nebraska
Date of amendment request: September 11, 2007.
Brief description of amendment: The amendment removed the footnote
to Technical Specification (TS) 2.3(4), ``Containment Sump Buffering
Agent Specification and Volume Requirement,'' and TS 3.6(2)d,
``Surveillance Requirements,'' limiting the applicability of those
specifications to operating cycle 24. Additionally, TS 2.3, figure 2-3
was revised to increase the volume of sodium tetraborate due to the
selection of a different chemical vendor and an increase in mass to
provide additional pH margin.
Date of issuance: March 25, 2008.
Effective date: The license amendment is effective as of its date
of issuance and shall be implemented prior to plant startup from the
2008 refueling outage.
Amendment No.: 253.
Renewed Facility Operating License No. DPR-40: The amendment
revised the Technical Specifications.
Date of initial notice in Federal Register: October 9, 2007 (72 CFR
57356). The Commission's related evaluation of the amendment is
contained in a safety evaluation dated March 25, 2008.
No significant hazards consideration comments received: No.
Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station,
Unit No. 1, Washington County, Nebraska
Date of amendment request: October 5, 2007.
Brief description of amendment: The amendment revised emergency
diesel generator (DG) surveillance testing in Technical Specification
(TS) 3.7, ``Emergency Power Systems,'' to support modification of the
DG start circuitry. Currently, TS 3.7 requires the licensee to verify
the anticipatory DG start-to-idle speed upon a reactor trip. This
amendment deletes the anticipatory DG starting requirement. The
amendment also deletes the footnote in TS 3.7.(1)e. that pertains to a
one-time extension of surveillance interval for DG-1 that was granted
in Amendment No. 112 to the Renewed Facility Operating License.
Date of issuance: March 26, 2008.
Effective date: As of its date of issuance and prior to startup
from the 2008 refueling outage.
Amendment No.: 254.
Renewed Facility Operating License No. DPR-40: The amendment
revised the Technical Specifications.
Date of initial notice in Federal Register: November 20, 2007 (72
FR 65369). The Commission's related evaluation of the amendment is
contained in a safety evaluation dated March 26, 2008.
No significant hazards consideration comments received: No.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-424 and 50-
425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of application for amendments: February 13, 2008, as
supplemented on March 21, and April 3, 2008.
Brief description of amendments: The amendments proposed a one-time
steam generator (SG) tubing eddy current inspection interval revision
to the Vogtle Electric Generating Plant, Units 1 and 2 (Vogtle 1 and 2)
Technical Specifications (TSs) 5.5.9, ``Steam Generator (SG) Program,''
to incorporate an interim alternate repair criterion in the provisions
for SG tube repair criteria during the Vogtle 1 inspection performed in
Refueling Outage 14 and subsequent operating cycle, and during the
Vogtle 2 inspection performed in Refueling Outage 13 and subsequent 18-
month SG tubing eddy current inspection interval and subsequent 36-
month SG tubing eddy current inspection interval. The amendments also
revised TS 5.6.10, ``Steam Generator Tube Inspection Report,''
[[Page 21667]]
where three new reporting requirements are proposed to be added to the
existing seven requirements.
Date of issuance: April 9, 2008.
Effective date: As of the date of issuance and shall be implemented
within 30 days from the date of issuance April 9, 2008.
Amendment Nos.: 150 and 130.
Facility Operating License Nos. NPF-68 and NPF-81: Amendments
revised the licenses and the technical specifications.
Date of initial notice in Federal Register: February 26, 2008 (73
FR 10305) The supplements dated March 21, and April 3, 2008, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the staff's original proposed no significant hazards consideration
determination. The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated April 9, 2008.
No significant hazards consideration comments received: No.
Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear Plant,
Unit 2, Hamilton County, Tennessee
Date of application for amendment: January 12, 2007, as
supplemented by letters dated January 8 and February 8, 2008.
Brief description of amendment: A Change to the Unit 2 Technical
Specifications (TS) to include a Steam Generator SG voltage-based
repair criteria probability of detection method using plant specific SG
tube inspection results. The revised method is referred to as the
Probability of Prior Cycle Detection method.
Date of issuance: March 24, 2008.
Effective date: As of the date of issuance and shall be implemented
within 45 days.
Amendment No.: 309.
Facility Operating License No. DPR-79: Amendment revises the
technical specifications.
Date of initial notice in Federal Register: March 13, 2007 (72 FR
11395). The supplemental letters dated January 8 and February 8, 2008,
provided additional information that clarified the application, did not
expand the scope of the application as originally noticed, and did not
change the staff's original proposed no significant hazards
consideration determination as published in the Federal Register. The
Commission's related evaluation of the amendment is contained in a
Safety Evaluation dated March 24, 2008.
No significant hazards consideration comments received: No.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of application for amendments: April 5, 2007.
Brief description of amendments: The technical specifications
change will revise the surveillance frequency for the turbine trip
functions of the reactor trip system instrumentation.
Date of issuance: April 2, 2008.
Effective date: As of the date of issuance and shall be implemented
within 45 days.
Amendment Nos.: 318 and 310.
Facility Operating License Nos. DPR-77 and DPR-79: Amendments
revised the technical specifications.
Date of initial notice in Federal Register: May 22, 2007 (72 FR
28723).
The Commission's related evaluation of the amendments is contained
in a safety evaluation dated April 2, 2008.
No significant hazards consideration comments received: No.
Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek
Generating Station, Coffey County, Kansas
Date of amendment request: March 14, 2007, as supplemented by
letters dated December 18, 2007, and February 26, 2008.
Brief description of amendment: The amendment revised Technical
Specification (TS) 3.3.2, ``Engineered Safety Features Actuation System
(ESFAS) Instrumentation,'' and TS 3.7.3, ``Main Feedwater Isolation
Valves (MFIVs),'' by the addition of the main feedwater regulating
valves (MFRVs), and associated MFRV bypass valves, to TS 3.7.3 and to
TS Table 3.3.2-1, and changed page numbers in the TS Table of Contents.
The application has one last proposed change to the plant, which is the
proposed modification of the Main Steam Feedwater Isolation System
controls. This will be addressed later in a future letter.
Date of issuance: April 3, 2008.
Effective date: Effective as of its date of issuance and shall be
implemented before entry into Mode 3 in the restart from the spring
2008 refueling outage.
Amendment No.: 177.
Facility Operating License No. NPF-42. The amendment revised the
Operating License and Technical Specifications.
Date of initial notice in Federal Register: June 19, 2007 (72 FR
33785). The supplemental letters dated December 18, 2007, and February
26, 2008, provided additional information that clarified the proposed
changes in the application, did not expand the scope of the application
as originally noticed, and did not change the NRC staff's original
proposed no significant hazards consideration determination published
in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated April 3, 2008.
No significant hazards consideration comments received: No.
Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek
Generating Station, Coffey County, Kansas
Date of amendment request: February 8, 2008, as supplemented by
letters dated March 21 and 30, 2008.
Brief description of amendment: The amendment revised Technical
Specification (TS) 5.5.9, ``Steam Generator (SG) Program,'' and TS
5.6.10, ``Steam Generator Tube Inspection Report.'' For TS 5.5.9, the
amendment would replace the existing alternate repair criteria (ARC) in
TS 5.5.9.c.1 for SG tube inspections that was approved in Amendment No.
169 issued October 10, 2006, for refueling outage 15 (the outage for
the fall of 2006) and the subsequent operating cycle. The new interim
ARC would be for the upcoming refueling outage 16 (the outage for the
spring of 2008) and the subsequent 18-month operating cycle, and would
apply to service-induced crack-like flaws found below 17 inches from
the top of the tubesheet. For TS 5.6.10, three new reporting
requirements are added to the existing seven requirements.
Date of issuance: April 4, 2008.
Effective date: Effective as of its date of issuance and shall be
implemented prior to the entry into Mode 4 during the startup from
refueling outage 16 in the spring of 2008.
Amendment No.: 178.
Facility Operating License No. NPF-42. The amendment revised the
Operating License and Technical Specifications.
Date of initial notice in Federal Register: February 21, 2008 (73
FR 9602). The supplemental letters dated March 21 and 30, 2008,
provided additional information that clarified the application, did not
expand the scope of the application as originally noticed, and did not
change the staff's original proposed no significant hazards
consideration determination as published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated April 4, 2008.
No significant hazards consideration comments received: No.
[[Page 21668]]
Dated at Rockville, Maryland, this 14th day of April 2008.
For The Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor Licensing, Office of Nuclear
Reactor Regulation.
[FR Doc. E8-8388 Filed 4-21-08; 8:45 am]
BILLING CODE 7590-01-P