[Federal Register Volume 60, Number 21 (Wednesday, February 1, 1995)]
[Notices]
[Pages 6296-6324]
From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
[FR Doc No: 95-2350]
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NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory
Commission (the Commission or NRC staff) is publishing this regular
biweekly notice. Public Law 97-415 revised section 189 of the Atomic
Energy Act of 1954, as amended (the Act), to require the Commission to
publish notice of any amendments issued, or proposed to be issued,
under a new provision of section 189 of the Act. This provision grants
the Commission the authority to issue and make immediately effective
any amendment to an operating license upon a determination by the
Commission that such amendment involves no significant hazards
consideration, notwithstanding the pendency before the Commission of a
request for a hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from January 5, 1995, through January 20, 1995.
The last biweekly notice was published on January 18, 1995 (60 FR
3669).
NOTICE OF CONSIDERATION OF ISSUANCE OF AMENDMENTS TO FACILITY OPERATING
LICENSES, PROPOSED NO SIGNIFICANT HAZARDS CONSIDERATION DETERMINATION,
AND OPPORTUNITY FOR A HEARING
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination.
Normally, the Commission will not issue the amendment until the
expiration of the 30-day notice period. However, should circumstances
change during the notice period such that failure to act in a timely
way would result, for example, in derating or shutdown of the facility,
the Commission may issue the license amendment before the expiration of
the 30-day notice period, provided that its final determination is that
the amendment involves no significant hazards consideration. The final
determination will consider all public and State comments received
before action is taken. Should the Commission take this action, it will
publish in the Federal Register a notice of issuance and provide for
opportunity for a hearing after issuance. The Commission expects that
the need to take this action will occur very infrequently.
Written comments may be submitted by mail to the Rules Review and
Directives Branch, Division of Freedom of Information and Publications
Services, Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555, and should cite the publication date and page
number of this Federal Register notice. Written comments may also be
delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland from 7:30 a.m. to 4:15 p.m. [[Page 6297]] Federal
workdays. Copies of written comments received may be examined at the
NRC Public Document Room, the Gelman Building, 2120 L Street, NW.,
Washington, DC. The filing of requests for a hearing and petitions for
leave to intervene is discussed below.
By March 3, 1995, the licensee may file a request for a hearing
with respect to issuance of the amendment to the subject facility
operating license and any person whose interest may be affected by this
proceeding and who wishes to participate as a party in the proceeding
must file a written request for a hearing and a petition for leave to
intervene. Requests for a hearing and a petition for leave to intervene
shall be filed in accordance with the Commission's ``Rules of Practice
for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested
persons should consult a current copy of 10 CFR 2.714 which is
available at the Commission's Public Document Room, the Gelman
Building, 2120 L Street, NW., Washington, DC and at the local public
document room for the particular facility involved. If a request for a
hearing or petition for leave to intervene is filed by the above date,
the Commission or an Atomic Safety and Licensing Board, designated by
the Commission or by the Chairman of the Atomic Safety and Licensing
Board Panel, will rule on the request and/or petition; and the
Secretary or the designated Atomic Safety and Licensing Board will
issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.714, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following factors: (1) The nature of the petitioner's right under the
Act to be made a party to the proceeding; (2) the nature and extent of
the petitioner's property, financial, or other interest in the
proceeding; and (3) the possible effect of any order which may be
entered in the proceeding on the petitioner's interest. The petition
should also identify the specific aspect(s) of the subject matter of
the proceeding as to which petitioner wishes to intervene. Any person
who has filed a petition for leave to intervene or who has been
admitted as a party may amend the petition without requesting leave of
the Board up to 15 days prior to the first prehearing conference
scheduled in the proceeding, but such an amended petition must satisfy
the specificity requirements described above.
Not later than 15 days prior to the first prehearing conference
scheduled in the proceeding, a petitioner shall file a supplement to
the petition to intervene which must include a list of the contentions
which are sought to be litigated in the matter. Each contention must
consist of a specific statement of the issue of law or fact to be
raised or controverted. In addition, the petitioner shall provide a
brief explanation of the bases of the contention and a concise
statement of the alleged facts or expert opinion which support the
contention and on which the petitioner intends to rely in proving the
contention at the hearing. The petitioner must also provide references
to those specific sources and documents of which the petitioner is
aware and on which the petitioner intends to rely to establish those
facts or expert opinion. Petitioner must provide sufficient information
to show that a genuine dispute exists with the applicant on a material
issue of law or fact. Contentions shall be limited to matters within
the scope of the amendment under consideration. The contention must be
one which, if proven, would entitle the petitioner to relief. A
petitioner who fails to file such a supplement which satisfies these
requirements with respect to at least one contention will not be
permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing, including the opportunity to present evidence and cross-
examine witnesses.
If a hearing is requested, the Commission will make a final
determination on the issue of no significant hazards consideration. The
final determination will serve to decide when the hearing is held.
If the final determination is that the amendment request involves
no significant hazards consideration, the Commission may issue the
amendment and make it immediately effective, notwithstanding the
request for a hearing. Any hearing held would take place after issuance
of the amendment.
If the final determination is that the amendment request involves a
significant hazards consideration, any hearing held would take place
before the issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed with the Secretary of the Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555, Attention: Docketing and Services
Branch, or may be delivered to the Commission's Public Document Room,
the Gelman Building, 2120 L Street, NW., Washington DC, by the above
date. Where petitions are filed during the last 10 days of the notice
period, it is requested that the petitioner promptly so inform the
Commission by a toll-free telephone call to Western Union at 1-(800)
248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator
should be given Datagram Identification Number N1023 and the following
message addressed to (Project Director): petitioner's name and
telephone number, date petition was mailed, plant name, and publication
date and page number of this Federal Register notice. A copy of the
petition should also be sent to the Office of the General Counsel, U.S.
Nuclear Regulatory Commission, Washington, DC 20555, and to the
attorney for the licensee.
Nontimely filings of petitions for leave to intervene, amended
petitions, supplemental petitions and/or requests for a hearing will
not be entertained absent a determination by the Commission, the
presiding officer or the Atomic Safety and Licensing Board that the
petition and/or request should be granted based upon a balancing of
factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's Public Document Room, the Gelman Building, 2120 L
Street, NW., Washington, DC, and at the local public document room for
the particular facility involved.
Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power
Station, Plymouth County, Massachusetts
Date of amendment request: November 22, 1994.
Description of amendment request: The proposed amendment would
increase the current Emergency Diesel Generator (EDG) allowed out-of-
service time in Specification 3.5.F from 72 hours to 7 days, deletes
the daily testing of the operable diesel generator in Specification
4.5.F.1, when it is determined that the other diesel generator is
inoperable, and revises specification 3.9.B.1 and 2 for EDG
operability.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
[[Page 6298]] (1) The proposed amendment does not involve a
significant increase in the probability of consequences of an
accident previously evaluated.
Operation of PNPS [Pilgrim Nuclear Power Station] in accordance
with the proposed license amendment will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
Implementation of the proposed change is expected to result in
an increase in the probability of core damage, from 5.85E-5/year
(this is the PNPS IPE [individual plant examination] core damage
frequency) to 5.88E-5/year. This increase is less than one percent
and is considered to be insignificant relative to the underlying
uncertainties involved with probabilistic risk assessments.
Deleting the testing requirement for an EDG when the other EDG
is in repair does not increase the probability or consequences of an
accident previously evaluated because the reliability program and
Technical Specification required surveillances continue to provide
the added assurance sought by the testing. The elimination of this
testing might improve the overall reliability of the EDGs.
(2) The proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
Operation of PNPS in accordance with the proposed license
amendment will not create the possibility of a new or different kind
of accident from any accident previously evaluated. No change is
being made in the manner in which the EDG's provide plant
protection. No new modes of plant operation are involved. Extending
the EDG OOS [out of service] and, deleting the testing requirement
for one EDG when the other EDG is in repair does not necessitate
physical alteration of the plant or changes in plant operational
limits.
3. The proposed amendment does not involve a significant
reduction in a margin of safety.
Operation of PNPS in accordance with the proposed license
amendment will not involve a significant reduction in a margin of
safety. [***], incorporation of the proposed change involves an
insignificant reduction in the margin of safety.
As previously stated, implementation of the proposed changes is
expected to result in an insignificant increase in: (1) power
unavailability to the emergency buses (given that a loss of offsite
power has occurred), and (2) core damage frequency. EDG reliability
improvement is expected due to increased quality and thoroughness of
EDG maintenance. Implementation of the proposed changes does not
increase the consequences of a previously analyzed accident nor
significantly reduce a margin of safety. Functioning of the EDGs and
the manner in which limiting condition of operability are
established are unaffected.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Plymouth Public Library, 11
North Street, Plymouth, Massachusetts 02360.
Attorney for licensee: W.S. Stowe, Esquire, Boston Edison Company,
800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
NRC Project Director: Walter R. Butler.
Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson
Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
Date of amendment request: December 27, 1994.
Description of amendment request: The requested Technical
Specifications (TS) change relocates the turbine rotor inspection
requirement, TS 4.1-3, Item 13, to the Updated Final Safety Analysis
Report (UFSAR), Section 10.2. This TS requires a turbine inspection,
including visual, magnaflux, and dye petrant inspections on a frequency
of every five years with a maximum time between tests of six years.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The requested change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated. The requested change relocates the turbine inspection
requirement from the TS to the UFSAR. Turbine inspections will
continue to be controlled and performed such that the low turbine
missile generation probability will be maintained. The consequences
of missile generation are unchanged since this change does not
involve the addition or modification of plant equipment, nor does it
alter the design or operation of plant systems. Therefore, there
would be no increase in the probability or consequences of an
accident previously evaluated.
2. The requested change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated. The requested change relocates the turbine inspection
requirement from the TS to the UFSAR. Turbine inspections will
continue to be controlled and performed such that the low turbine
missile generation probability will be maintained. This change does
not involve the addition or modification of plant equipment, nor
does it alter the design or operation of plant systems. Therefore,
the proposed changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. The requested change does not involve a significant reduction
in the margin of safety. The requested change relocates the turbine
inspection requirement from the TS to the UFSAR. Turbine inspections
will continue to be controlled and performed such that the low
turbine missile generation probability will be maintained.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Hartsville Memorial Library,
147 West College Avenue, Hartsville, South Carolina 29550.
Attorney for licensee: R. E. Jones, General Counsel, Carolina Power
& Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
NRC Project Director: William H. Bateman.
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties,
North Carolina
Date of amendment request: December 19, 1994.
Description of amendment request: The proposed one-time schedular
extension would allow the third test of the first 10-year service
period to be performed during refueling outage no. 7, at approximately
a 54 month interval instead of the current maximum Technical
Specification interval of 50 months, and coincident with the 10-year
service period to be performed during refueling outage no. 7 and the
10-year inservice inspection,
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
This [extension] request applies to the ILRT [integrated leak
rate testing] and does not affect the local leak rate testing of
containment penetrations and isolation valves where the majority of
the leakage occurs. The allowable containment leakage used in the
accident analysis for offsite doses, La, is 0.1 [weight percent
per day] and for conservatism the leakage is limited to 75 percent
La at startup to account for the possible degradation of
containment leakage barriers between two ILRT tests. Based on the
``as left'' leakage data for the past two ILRTs, the additional time
period added to the testing interval would not adversely impact the
containment leakage barriers to the extent [[Page 6299]] that
degradation would cause leakage to exceed that assumed in the
accident analysis.
2. The proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The change to the Surveillance Requirement is a one time
[extension] to extend the surveillance interval from the maximum of
50 months to approximately 54 months for performance of the third
ILRT in the first service period. There are no design changes being
made that would create a new type of accident or malfunction and the
method and manner of plant operation remain unchanged. Extension of
the surveillance interval for performing the ILRT does not adversely
impact the surveillances ability to show that containment integrity
is maintained.
3. The proposed amendment does not involve a significant
reduction in the margin of safety.
There are no changes being made to the safety limits or safety
system settings that would adversely impact plant safety. The change
is a one time [extension] to extend the time interval for performing
an ILRT approximately four months beyond the current maximum
interval. In addition to the indication of continued containment
integrity provided by the Local Leak Rate Testing program, the
surveillance test data from the first and second ILRTs illustrates
that there is sufficient leakage margin to remain well below the
allowable leakage rate of La. The as-left leakage rate for the
last ILRT was 0.0614 [weight percent per day], which is well below
the 0.075 [weight percent per day] allowed by the T.S., and
therefore provides margin for degradation that is greater than the
minimum provided by the Technical Specifications. Therefore, this
change does not significantly reduce the margin of safety for
Technical Specification 3.6.1.2.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Cameron Village Regional
Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
Attorney for licensee: R. E. Jones, General Counsel, Carolina Power
& Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
NRC Project Director: William H. Bateman.
Consumers Power Company, Docket No. 50-255, Palisades Plant, Van
Buren County, Michigan
Date of amendment request: December 29, 1994.
Description of amendment request: The proposed amendment would
affect the method of controlling the pH of the post-LOCA containment
sump solution by allowing the replacement of the existing operator
actuated Iodine Removal System with a passive system of baskets of
Trisodium Phosphate (TSP) in the lower regions of the containment. The
current Iodine Removal System provides sodium hydroxide (NaOH) for
injection into the containment spray to maintain pH of the sump
solution.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
The following evaluation supports the finding that operation of the
facility in accordance with the proposed change from NaOH to TSP
requirements would not:
1. Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The substitution of TSP baskets for the NaOH addition equipment
would not cause any changes to the capability, settings, or
operation of the plant systems (other than the Iodine Removal System
itself) and would not, therefore, have any effect on the probability
of occurrence of an accident.
The substitution of TSP baskets for the NaOH addition equipment
has the effect of providing more immediate control of post-LOCA sump
pH, thereby increasing the assurance that iodine will remain in
solution throughout a postulated event. The consequences of
accidents evaluated in the FSAR [Final Safety Analysis Report] will
not be increased by this increased assurance.
2. Create the possibility of a new or different kind of accident
from any previously evaluated.
The TSP baskets are passive components which have no interaction
with plant equipment unless flooding occurs in the containment. They
are designed and located such that they will not interact with any
plant safety equipment during a seismic event. The NaOH equipment,
which will be replaced by the TSP baskets, has no function or effect
on other equipment except during accident conditions. Therefore, the
substitution of TSP baskets for NaOH addition equipment cannot
create the possibility of a new or different kind of accident from
any previously evaluated.
3. Involve a significant reduction in a margin of safety.
The substitution of TSP baskets for the NaOH addition equipment
would assure that the sump pH at the initiation of RAS
[recirculation actuation signal] is between 7.0 and 8.0 as assumed
in the MHA [maximum hypothetical accident] analysis. Therefore, this
change would not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Van Wylen Library, Hope
College, Holland, Michigan 49423.
Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power
Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
NRC Project Director: John N. Hannon.
Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment request: December 7, 1994.
Description of amendment request: The amendments revise the
Technical Specification action statement to allow the Control Room Air
Intake to remain open when radiation monitors (EMF-43A and EMF-43B) are
inoperable. Immediate action to return the monitors to service would be
required.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment would not involve a significant
increase in the probability or consequences of any accident
previously evaluated in the FSAR [Final Safety Analysis Report].
The amendment change will ensure correct Control Room
Ventilation system alignment in order to mitigate the consequence of
a Design Basis LOCA as described in FSAR Section 15.6.5.3,
Environmental Consequences of a Loss of-Coolant Accidents, Control
Room Operator Dose.
The amendment change will permit the intake to remain open and
will specify that action to repair the affected monitor shall be
taken immediately. The change itself is not considered to be an
initiator of any previously evaluated accident. Maintaining the VC
intake open with an inoperable monitor will not result in any
accidents that have not been previously evaluated. The
implementation of immediate actions to repair the inoperable monitor
does not in itself represent any accidents that have not been
previously evaluated. Therefore, the proposed Technical
Specification change does not increase the occurrence probability of
previously evaluated accidents.
The change to permit maintenance of open intakes will not
increase the consequences of any previously evaluated accidents. The
proposed amendment change is consistent with the original Safety
Analysis concerning the Dose to the Operators.
The analysis determined that the Doses to the Operators were
within acceptable ranges given the assumptions that the intakes
would [[Page 6300]] remain open and the contaminated air was
processed through a Safety Related filter train prior to
introduction into the Control Room. The proposed change remains
consistent with this analysis and does not change the assumptions or
methodology utilized to assess the Doses to the Operators for a
hypothesized DBA; therefore, the proposed amendment change will not
increase the consequences of any previously evaluated accident.
2. The proposed amendment would not create the possibility of a
new or different kind of accident not previously evaluated.
The proposed change will not modify, delete, or add any systems
or components; therefore, no new failure modes or accidents
scenarios will be created.
No test or experiments will be revised; therefore, no new
initiating events or unanalyzed condition will be created.
Administrative changes to surveillance procedures will be minor and
will not create a safety concern.
3. No significant reduction in a margin of safety will occur.
The proposed amendment change requiring immediate action to
initiate repairs to an inoperable monitor does not impact existing
Safety Margins. Since requirements for immediate corrective action
does not currently exist within the Specification, the changes will
enhance the availability of the subject monitors.
The proposed amendment does not change/impact any assumption or
methods utilized to assess the doses to the operators for a
hypothetical worst case DBA. Accordingly, the proposed amendment
does not reduce any safety margins.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Atkins Library, University of
North Carolina, Charlotte (UNCC Station), North Carolina 28223.
Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422
South Church Street, Charlotte, North Carolina 28242.
NRC Project Director: Herbert N. Berkow.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric
Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: December 9, 1994.
Description of amendment request: The proposed amendment would
revise the technical specifications (TSs) by revising the allowable
opening tolerances on the Pressurizer Code Safety Valves and the Main
Steam Line Code Safety Valves from plus or minus 1% to plus or minus
3%. This request is submitted as a result of an effort to improve valve
performance and to ensure that the TS limits are consistent with
expected valve performance capabilities.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve any change to the
physical characteristics of the PSVs [pressurizer safety valves] and
MSSVs [main steam safety valves] and will have no impact on the PSVs
and MSSVs as-left setting. This change only allows for a larger
(plus or minus 3% versus plus or minus 1%) as-found setpoint
tolerance. Therefore, this change has no impact on the probability
of occurrence of any accident previously evaluated. The impact of
this change on the FSAR [final safety analyses report] analyses has
been evaluated and the results of the impacted events have been
found to be within the acceptable limits.
Therefore, revising the PSV and MSSV as-found opening setpoint
tolerance from plus or minus 1% to plus or minus 3% does not
increase the probability or consequences of an accident previously
evaluated.
2. The proposed changes to the PSVs and MSSVs as-found opening
setpoint tolerance do not modify equipment or change the manner in
which the plant will be operated. The safety valves will continue to
function per their design. Since no hardware modifications or
changes in operation procedures will be made, the proposed changes
will not create the possibility of a new or different kind of
accident from any accident previously evaluated.
3. The impact of the proposed changes on the Waterford 3 FSAR
analyses have been evaluated. The evaluation demonstrates that the
results of the impacted events remained within the acceptable
limits. The system capabilities to mitigate and/or prevent accidents
will be the same as they were prior to these changes. Therefore, the
proposed changes do not involve a reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room Location: University of New Orleans
Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L
Street N.W., Washington, D.C. 20005-3502.
NRC Project Director: William D. Beckner.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam
Electric Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: December 9, 1994.
Description of amendment request: The proposed amendment would
revise the technical specifications (TSs) by revising a plant
protection system (PPS) trip setpoint and several allowable values such
that they will be consistent with the current setpoint/uncertainty
methodology being implemented at Waterford 3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Implementing the proposed change will not affect any design
basis accident. The revised Trip Setpoint and Allowable Values are
based upon the same Analytical Limits that form the basis for the
current Trip Setpoints and Allowable Values. The design basis for
each Trip Setpoint was verified to be consistent with the
appropriate accident analyses as part of the process of revising the
PPS setpoint analysis. The proposed change would implement a new
Trip Setpoint for the Reactor Coolant (RC) System Low Flow Reactor
trip and new Allowable Values for RC Low Flow, HI Log Power, HI
Steam Generator Water Level, HI Containment Pressure, Low
Pressurizer Pressure, Low Steam Generator Pressure, Low Steam
Generator Water Level, and Low RWSP [refueling water storage pool]
Level, based on the results of calculation EC-I92-019. The revised
Low RC Flow Trip Setpoint is based on the same analytical limit as
the current setpoint. The revised calculation uses the same design
inputs with a similarly based methodology to calculate a smaller
loop uncertainty. This results in a revised RC Low Flow Trip
Setpoint that retains the original analysis limit. Therefore, the
proposed change will not involve a significant increase in the
probability or consequences of any previously analyzed accident.
Plant operation and the manner in which the plant is operated
will not be altered as a result of implementing the proposed change
since no new system or design change is being implemented. The
proposed Setpoint and Allowable Value changes do not create any new
system interactions or interfaces. All information used to calculate
the new Trip Setpoint is consistent with that of the existing
accident analyses, and no new system interfaces/interactions are
created. Therefore, the proposed change will not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
The proposed setpoint change revised the point at which the RCS
Low Flow reactor trip initiates a reactor trip. The Trip Setpoint is
based on the same Analytical Limit used to determine the current
setpoint. In addition, the same basic setpoint determination
[[Page 6301]] methodology is employed. That is, the Trip Setpoint is
the Analytical Limit plus or minus the Total Loop Uncertainty [TLU].
The Allowable Value is the Trip Setpoint plus or minus the Periodic
Test Error [PTE]. The change in the setpoint and allowable values
are [sic] due to a change in calculated TLU and PTE. The proposed
Trip Setpoint and Allowable Values are based on the same Analytical
Limits for the affected parameters and are determined using approved
methodology. Therefore, the proposed change will not involve a
significant reduction in margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room Location: University of New Orleans
Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L
Street N.W., Washington, D.C. 20005-3502.
NRC Project Director: William D. Beckner.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of amendment request: December 27, 1994.
Description of amendment request: The proposed amendments would
revise the period for conducting leak testing of containment purge
valves to every refueling outage.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change to the Technical Specifications does not
involve a significant increase in the probability or consequences of
an accident previously evaluated because the [test] results have
demonstrated that the resilient seat material does not degrade and
cause containment isolation valves to leak. Therefore the valves
will perform as assumed in the accident analyses.
2. The proposed change to the Technical Specifications does not
create the possibility of a new or different kind of accident from
any accident previously evaluated because it does not require the
valves to function in any manner other than that which is currently
required.
3. The proposed addition to the Technical Specifications does
not involve a significant reduction in a margin of safety because it
only affects the frequency of the test and does not change the
leakage acceptance criteria. Since sufficient data has been
collected to demonstrate that the resilient seals do not degrade,
testing at the same frequency as other containment isolation valves
will not reduce the margin of safety provided by the Technical
Specifications.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Burke County Public Library,
412 Fourth Street, Waynesboro, Georgia 30830.
Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta,
Georgia 30308.
NRC Project Director: Herbert N. Berkow.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of amendment request: December 29, 1994.
Description of amendment request: This request withdraws a similar
request dated January 22, 1993, as supplemented August 8, 1993, and
submits a new one in its place. The proposed amendments would revise
the Technical Specifications (TS) to add the automatic load sequencer
specification to TS Section 3/4.3, Instrumentation, and associated
Bases, and TS Section 3/4.8, Electrical Power Systems.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change to the Technical Specifications does not
involve a significant increase in the probability or consequences of
an accident previously evaluated because the action to be taken when
an automatic load sequencer is inoperable is consistent with that of
a more stringent condition already specified, namely, the loss of an
entire train of emergency power during Modes 1-4, and for Modes 5
and 6 adding specific actions which previously had never been
addressed in TS.
2. The proposed change to the Technical Specifications does not
create the possibility of a new or different kind of accident from
any accident previously evaluated because it does not involve any
change to the design, operation, or performance of the automatic
load sequencer. It only serves to clearly identify the appropriate
conservative response to an inoperable automatic load sequencer
applicable to the plant mode of operation.
3. The proposed change to the Technical Specifications does not
involve a significant reduction in a margin of safety because the
proposed actions to take when an automatic load sequencer is
inoperable [are] the same as the action already required by the
Technical Specifications when no power is available to the entire
emergency bus during Modes 1-4 and by adding requirements during
Modes 5 and 6, which had previously never been addressed.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Burke County Public Library,
412 Fourth Street, Waynesboro, Georgia 30830.
Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta,
Georgia 30308.
NRC Project Director: Herbert N. Berkow.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of amendment request: January 3, 1995.
Description of amendment request: The proposed amendments would
revise the Technical Specifications (TS) with editorial changes to the
Action Statements of TS Sections 3.8.1.1 and 3.8.1.2 in order to
reflect the availability of a third offsite ac electrical source.
Surveillance Requirement 4.8.1.1.1 is being clarified to distinguish
that the offsite ac circuits which are connected to the onsite Class 1E
distribution system are required to be verified OPERABLE. The
amendments also modify the Technical Specifications with the addition
of a footnote to TS Section 3.8.3.1, to allow the connection of the
third offsite ac source to the onsite busses.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below: [[Page 6302]]
Based on the considerations regarding the addition of a footnote
for proper bus alignment during operating conditions, the licensee
submitted the following analysis in accordance with 10 CFR 50.92.
1. The proposed change to the Technical Specifications does not
involve a significant increase in the probability or consequences of
an accident previously evaluated because the probability of an LOSP
or an SBO is not increased by the allowance of having both redundant
emergency busses of 4160 volt switchgear connected to one offsite
source (RAT). The probability of having an LOSP is not increased
since the TS currently allow for a 72 hour LCO for one offsite power
source and the time the two redundant 4160 volt safety busses will
be temporarily aligned to one RAT is well within this time frame.
During this time the busses are interconnected, each bus is provided
adequate protection and separation by having separate and redundant
Class 1E circuit breakers, one per bus. The probability of an SBO is
not increased since neither bus' EDG will be affected during this
operation, and since this is a proceduralized manual alignment, the
interconnection to one RAT will not be initiated if either EDG were
inoperable. Also, the addition of the new ``swing'' offsite power
source (SAT), increases availability and flexibility of the VEGP
response to either an LOSP or SBO.
2. The proposed change to the Technical Specifications does not
create the possibility of a new or different kind of accident from
any accident previously evaluated because the only postulated
adverse consequences of tying both redundant 4160 volt safety busses
together to one RAT is an LOSP. An LOSP is a design basis event
which has already been analyzed for VEGP. In response to an LOSP,
both EDGs remain capable of carrying the required loads to mitigate
the consequences of any postulated design basis accident during or
coincident with an LOSP.
3. The proposed addition to the Technical Specifications does
not involve a significant reduction in a margin of safety because
the only accident mitigating equipment and/or power sources which
will be unavailable during the transfer of offsite power sources is
the offsite power source being removed from service, allowed by
existing TS LCO 3.8.1.1(a). The 13.8 kV loads associated with the
RAT being removed from service and all of the 4160 volt non-Class 1E
loads fed from either RAT will be unavailable during this temporary
alignment. All of these loads are nonsafety related and therefore
are enveloped by the existing LOSP analysis.
Based on the considerations regarding clarification of SAT Use and
Expanded Bases, the licensee submitted the following analysis in
accordance with 10 CFR 50.92.
1. The proposed change to the TS does not involve a significant
increase in the probability or consequences of an accident
previously evaluated because only clarifications to existing TS
action statements and an additional expanded bases are being made.
No changes to the existing TS requirements for A.C. sources are
being made. The safety function of the offsite power source is
unchanged by the addition of the SAT and the probability of an LOSP
or SBO is not increased. In actuality, the addition of the SAT
increases the availability and flexibility of VEGP responses to
either an LOSP or SBO.
2. The proposed change to the TS does not create the possibility
of a new or different kind of accident from any accident previously
evaluated because the loss of the SAT while being utilized to meet
TS offsite power source requirements is enveloped by existing LOSP
analysis.
3. The proposed change does not involve a significant reduction
in a margin of safety because although the SAT has no 13.8 kV
secondary winding, nor the same capacity as a RAT for accepting 4.16
kV non Class 1E loads, these loads are nonsafety related and
therefore enveloped by existing analysis. If a unit trip were to
occur while one 4.16 kV safety bus is being powered from the SAT,
the effect is a loss of the 13.8 kV and non Class 1E 4.16 kV loads
associated with the out of service RAT. This scenario is enveloped
by existing LOSP analysis.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Burke County Public Library,
412 Fourth Street, Waynesboro, Georgia 30830.
Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta,
Georgia 30308
NRC Project Director: Herbert N. Berkow.
Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald
C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
Date of amendment requests: August 12, 1992 and supplemented April
12, 1993.
Description of amendment requests: The proposed amendments would
change the minimum channels operable for the pressurizer safety valve
position indicator acoustic monitor to two out of three total from one
per valve. The amendments also delete footnotes which are no longer
applicable.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
We [the licensee] have evaluated the proposed T/Ss exemption and
have determined that it should not require a significant hazards
consideration based on the criteria established in 10CFR50.92(c).
Operation of the Cook Nuclear Plant in accordance with the proposed
amendment will not:
(1) Involve a significant increase in the probability or
consequences of an accident previously evaluated.
Although the proposed exemption results in the operator having
one less source of information on plant status, it does not create a
significant increase in the probability or consequences of an
accident previously evaluated. The acoustic monitors do not perform
a function vital to safe shutdown or to the isolation of the
reactor, or the reactor coolant system pressure boundary, nor is
there a mechanism involving an operable or inoperable pressurizer
safety valve acoustic monitor which would initiate an accident.
These monitors were added to meet the requirements of NUREG-0578 and
NUREG-0737. During normal operations, other instrumentation exists
that provides the operator with indication of safety valve
actuation. The acoustic monitors are not necessary to and are not
used in the emergency operating procedures. In addition, the
acoustic monitors being inoperable will not result in an
uncontrolled release of radiation to the environment and will not
initiate an accident. Finally, although the operator may have one
less channel operable, the operator receives no less information
than if all three channels are operable because one valve opening
causes all operable channels to actuate. Therefore, we conclude that
the proposed T/Ss changes do not involve a significant increase in
the probability or consequences of an accident previously evaluated.
(2) Create the possibility of a new or different kind of
accident from any previously analyzed.
As previously stated, the purpose of the acoustic monitor is to
provide the operator with information regarding safety valve
position that may assist in the mitigation of the consequences of an
accident. Specifically, it provides information that a safety valve
has lifted. However, the operator has other mechanisms for obtaining
equivalent information. In addition, the signals generated by an
acoustic monitor do not initiate any other equipment actuation, nor
will the inoperability of an acoustic monitor initiate any accident.
Consequently, the proposed T/Ss changes do not create the
possibility of a new or different kind of accident from any
previously analyzed.
(3) Involve a significant reduction in a margin of safety.
The proposed T/Ss changes result in the operator potentially
having one less source of information on plant status. However, we
believe the margin of safety is not reduced for several reasons.
First, the operator is provided with other viable flow detection
devices to determine pressurizer safety valve position, i.e., the
temperature sensor on the discharge line associated with the
inoperable acoustic monitor, and pressurizer relief tank level (NLA-
351), temperature (NTA-351) [[Page 6303]] and pressure (NPA-351)
indications. Also, the acoustic monitors are not used by the
operators in an emergency situation, as the operator relies on other
indications of loss of reactor coolant inventory per the emergency
operating procedures. In addition, previous experience with the
pressurizer safety valve position indicator acoustic monitoring
system has shown that, when any one of the pressurizer safety valves
opens, all three safety valve position indicator acoustic monitors
are actuated. Because of this, the operator receives no less
information regardless if only two or three channels are operable.
Based on the above, we believe that having an acoustic monitor
inoperable does not warrant reactor and plant shutdown. As the T/Ss
are currently stated, should one pressurizer safety valve position
indicator acoustic monitor become inoperable, it must be restored to
operable status within thirty days or the unit must be in hot
shutdown within the subsequent twelve hours. Thermal cycling from
unwarranted plant shutdowns increases the likelihood of reactor
vessel embrittlement and unnecessarily challenges the safety
systems. Because a signal from the pressurizer safety valve position
indicator acoustic monitors is not necessary nor used to ensure the
safe shutdown of the unit even if a pressurizer safety valve is
opened or stuck open during an emergency situation, we believe that
a plant shutdown due to an inoperable acoustic monitor would be
unwarranted.
We believe that the unit can be operated safely and that we
would still meet the intent of NUREG-0538 and NUREG-0737 with only
two out of three pressurizer safety valve position indicator
acoustic monitors operable.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: Maud Preston Palenske Memorial
Library, 500 Market Street, St. Joseph, Michigan 49085.
Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts
and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
NRC Project Director: John N. Hannon.
Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee
Atomic Power Station, Lincoln County, Maine
Date of amendment request: November 18, 1994.
Description of amendment request: The proposed amendment would
change the title of certain Plant Operation Review Committee (PORC)
members to reflect recent Maine Yankee organizational changes; update
training requirements to comply with 10 CFR 50.120, Training and
qualification of nuclear power plant personnel; and reporting frequency
requirements for the Radioactive Effluent Release and Estimated Dose
and Meteorological Summary Reports.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration. The NRC staff has reviewed the licensee's analysis
against the standards of 10 CFR 50.92(c). A summary of the licensee's
analysis is presented below:
1. The proposed amendment would not involve a significant increase
in the probability or consequences of an accident previously evaluated.
The changes proposed by this amendment request are administrative
in nature. Because the proposed changes do not involve any physical
alterations to plant equipment, operating setpoints, parameters or
conditions, the plant's response to previously evaluated accidents is
not affected.
The licensee therefore concludes that implementation of the
proposed change will not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. The proposed amendment would not create the possibility of a new
or different kind of accident from any accident previously evaluated.
The administrative nature of the proposed changes does not affect
the design, operation, maintenance or testing of the plant. Thus, no
new modes of failure are created.
The licensee therefore concludes that implementation of the
proposed change will not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. The proposed amendment would not involve a significant reduction
in a margin of safety.
The proposed change reflects an organizational change that does not
modify the qualification requirements or competence of the members of
the PORC. Thus, the capability of PORC to meet its responsibilities in
accordance with the plant Technical Specifications is unchanged.
Deleting the current training requirement for Shift Technical
Advisors eliminates duplicative training requirements and represents
conformance to 10 CFR 50.120, Training and qualification of nuclear
power plant personnel.
Elevating the responsibility for training the plant staff from the
Manager, Operations Department, to the Vice President of Operations,
does not represent a reduction in a margin of safety.
The proposed change to the Radioactive Effluent Release and
Estimated Dose and Meteorological Summary Reports is related to the
submittal schedule for statistical data and is administrative in
nature. The change in submittal frequency provides consistency between
the various required reports and also is administrative in nature.
The licensee therefore concludes that implementation of the
proposed change would not involve a significant reduction in a margin
of safety.
Based on this review, it appears that the three standards of 10 CFR
50.92(c) are satisfied. Therefore, the NRC staff proposes to determine
that the amendment request involves no significant hazards
consideration.
Local Public Document Room location: Wiscasset Public Library, High
Street, P.O. Box 367, Wiscasset, Maine 04578.
Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic
Power Company, 329 Bath Road, Brunswick, Maine 04011.
NRC Project Director: Walter R. Butler.
Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone
Nuclear Power Station, Unit No. 2, New London County, Connecticut
Date of amendment request: December 16, 1994.
Description of amendment request: The proposed change to the
Technical Specifications would require the wind direction and wind
speed sensors at the 142 foot elevation to identify the data to
determine action required to preclude flood damage to the Service Water
Pumps. Also, the proposed change would correct a typographical error in
the location of the sensors at the 374 foot elevation.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
* * * The proposed changes do not involve a significant hazards
consideration because the changes would not:
1. Involve a significant increase in the probability or
consequences of an accident previously analyzed.
NNECO [Northeast Nuclear Energy Company] is proposing to revise
LCOs [Limiting Conditions for Operation] 3.7.5.1.b.3 and 3.7.5.1.b.4
and Table 3.3-8 of the Millstone Unit No. 2 Technical
[[Page 6304]] Specifications by changing the elevation that the
average wind speed and average wind direction are measured and by
correcting a typographical error, respectively. The proposed changes
have no effect on any of the accidents analyzed in Chapter 14 of the
Millstone Unit No. 2 FSAR [Final Safety Analysis Report]. Site
flooding is considered in Section 2.5.4.2.1 of the FSAR. Utilizing
the wind speed indicator at the 142-foot elevation, in lieu of the
indicator on the 374-foot elevation will not significantly change
the ability of personnel to predict the potential for a major storm
with flooding.
The proposed changes do not alter the intent of the
surveillances, do not involve any physical changes to the plant, do
not alter the way any structure, system, or component functions, and
do not modify the manner in which the plant is operated.
Based on the above, the proposed changes do not involve a
significant increase in the probability or consequences of an
accident previously analyzed.
2. Create the possibility of a new or different kind of accident
from any previously analyzed.
NNECO is proposing to revise LCOs 3.7.5.1.b.3 and 3.7.5.1.b.4
and Table 3.3-8 of the Millstone Unit No. 2 Technical Specifications
by changing the elevation that the average wind speed and average
wind direction are measured and by correcting a typographical error,
respectively. The proposed changes do not alter the intent of the
surveillances, do not involve any physical changes to the plant, do
not alter the way any structure, system, or component functions, and
do not modify the manner in which the plant is operated.
While the proposed changes to LCOs 3.7.5.1.b.3 and 3.7.5.1.b.4
do change the measurement location stipulated by the technical
specifications, this change is insignificant. Utilizing the wind
speed indicator at the 142-foot elevation, in lieu of the indicator
on the 374-foot elevation will not significantly change the ability
of personnel to predict the potential for a major storm with
flooding.
Based on the above, the proposed changes do not create the
possibility of a new or different kind of accident from any
previously analyzed.
3. Involve a significant reduction in a margin of safety.
NNECO is proposing to revise LCOs 3.7.5.1.b.3 and 3.7.5.1.b.4
and Table 3.3-8 of the Millstone Unit No. 2 Technical Specifications
by changing the elevation that the average wind speed and average
wind direction are measured and by correcting a typographical error,
respectively. The proposed changes will have no impact on the
physical protective boundaries (fuel matrix/cladding, reactor
coolant system pressure boundary, and containment). The proposed
changes do not alter the intent of the surveillances, do not involve
any physical changes to the plant, do not alter the way any
structure, system, or component functions, and do not modify the
manner in which the plant is operated.
While the proposed changes to LCOs 3.7.5.1.b.3 and 3.7.5.1.b.4
do change the manner in which potential flooding is predicted, this
change is insignificant. Utilizing the wind speed and direction
indicators at the 142-foot elevation, in lieu of the indicators at
the 374-foot elevation will not significantly change the ability of
personnel to predict the potential for a major storm with flooding.
Based on the above, the proposed changes do not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local public document room location: Learning Resource Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel,
Northeast Utilities Service Company, Post Office Box 270, Hartford, CT
06141-0270.
NRC Project Director: Phillip F. McKee.
Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone
Nuclear Power Station, Unit No. 2, New London County, Connecticut
Date of amendment request: December 21, 1994.
Description of amendment request: Proposed revision to License
Condition and Technical Specifications to relocate the Fire Protection
Requirements from the Technical Specifications to another controlled
document, the technical requirements manual (TRM).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
* * * The proposed changes do not involve a significant hazards
consideration because the changes would not:
1. Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The proposed changes relocates the provisions of the Fire
Protection Program that are contained in the Technical
Specifications and places them in the TRM. No current requirements
are being added or deleted aside from removal of the special reports
section. Review of the Fire Protection Program and its revisions
will be the responsibility of the PORC [Plant Operations Review
Committee] and SORC [Station Operations Review Committee], just as
it has always been the responsibility of these groups to review
changes to the fire protection Limiting Condition for Operation and
Surveillance Requirements when they were part of the Technical
Specifications. In addition, no design basis accidents are affected
by this change, nor are safety systems adversely affected by the
changes. Therefore, there is no impact on the probability of
occurrence or the consequences of any design basis accidents.
2. Create the possibility of a new or different kind of accident
from any previously evaluated.
The proposed changes relocate the provisions of the Fire
Protection Program that are contained in the Technical
Specifications and places them in the TRM. No current requirements
are being added or deleted aside from removal of the special report
section. There are no new failure modes associated with the proposed
changes. Since the plant will continue to operate as designed, the
proposed changes will not modify the plant response to the point
where it can be considered a new accident.
3. Involve a significant reduction in a margin of safety.
No change is being proposed for the Fire Protection Program
requirements themselves. The relevant Technical Specifications are
being relocated, and the requirements contained therein are being
incorporated into the TRM. Plant procedures will continue to provide
the specific instructions necessary for the implementation of the
requirements, just as when the requirements resided in the Technical
Specifications. Fire Protection Program changes will be governed by
the provisions of 10 CFR 50.59 and the current fire protection
license condition. As such, the changes do not directly affect any
protective boundaries nor does it impact the safety limits for the
boundary. Thus, there are no adverse impacts on the protective
boundaries, safety limits, or margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Learning Resource Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel,
Northeast Utilities Service Company, Post Office Box 270, Hartford, CT
06141-0270.
NRC Project Director: Phillip F. McKee.
Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone
Nuclear Power Station, Unit No. 3, New London County, Connecticut
Date of amendment request: December 2, 1994.
Description of amendment request: The proposed amendment modifies
the [[Page 6305]] surveillance requirements for the power range neutron
flux instrumentation to permit entering reactor operating modes 1 and 2
to perform necessary test for power range detectors.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration (SHC), which is presented below:
* * * The proposed changes do not involve an SHC because the
changes would not:
1. Involve a significant increase in the probability or
consequence of an accident previously analyzed.
NNECO is proposing to modify Table 4.3-1 by adding Note 5 to
Functional Units 2b, 3, and 4. This note provides an exception from
the provisions of Technical Specification 4.0.4. Entry into Mode 2
or Mode 1, as appropriate, would allow for appropriate test
conditions to complete the channel calibration of power range
neutron detectors (i.e., Functional Units 2b, 3, and 4 of Table 4.3-
1). This will improve plant safety by performing tests at proper
conditions. The acceptance criteria, such as response times, test
frequency, or test methods, are not revised. Therefore, the power
range neutron detectors will perform their intended function when
called upon. Additionally, the proposed changes are consistent with
the new, improved STS for the Westinghouse plants (NUREG-1431).
Based on the above, the proposed changes to Functional Units 2b,
3, and 4 of Table 4.3-1 of the Millstone Unit No. 3 Technical
Specifications do not involve a significant increase in the
probability or consequences of an accident previously analyzed.
2. Create the possibility of a new or different kind of accident
from any previously analyzed.
The proposed changes to Functional Units 2b, 3, and 4 of Table
4.3-1 do not make any physical or operational changes to existing
plant structures, systems, or components. The proposed changes do
not introduce any new failure mode. They simply allow tests to be
performed at appropriate conditions (e.g., Mode 2 or Mode 1 rather
than Mode 4 or Mode 3).
Additionally, the proposed changes do not modify the acceptance
criteria for the tests. The purpose of the tests is to ensure that
the power range neutron detectors can perform their intended
function.
Thus, the proposed changes do not create the possibility of a
new or different kind of accident from any previously analyzed.
3. Involve a significant reduction in the margin of safety.
The proposed changes to Functional Units 2b, 3, and 4 of Table
4.3-1 do not have any adverse impact on the design basis accident
analyses. The applicable acceptance criteria for the power range
neutron detectors will not be modified by the proposed changes. The
proposed changes will permit the tests to be conducted under the
proper conditions, so that the ability of the power range neutron
detectors to perform their intended safety function can be
confirmed.
Based on the above, there is no significant reduction in the
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Learning Resource Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel,
Northeast Utilities Service Company, Post Office Box 270, Hartford, CT
06141-0270.
NRC Project Director: Phillip F. McKee.
Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County,
Minnesota
Date of amendment requests: August 30, 1994.
Description of amendment requests: The proposed amendments would
revise the Technical Specifications (TS) for Prairie Island Nuclear
Generating Plant as recommended by Generic Letter (GL) 93-05, ``Line-
Item Technical Specification Improvements to Reduce Surveillance
Requirements for Testing During Power Operation.'' The proposed
amendments would also revise testing and calibration requirements
associated with the containment hydrogen recombiners. The proposed TS
changes are as follows:
(1) TS Table 4.1-1C, ``Miscellaneous Instrumentation Surveillance
Requirements.'' Delete Item 14, ``Accumulator Level and Pressure'' and
corresponding frequency interval designations.
(2) TS Table 4.1-2A, ``Minimum Frequencies For Equipment Tests,''
Item 2. Revise the frequency for partial movement of all control rod
assemblies from every 2 weeks to once per quarter.
(3) TS 4.3, ``Primary Coolant System Pressure Isolation Values.''
Under Specification heading, extend the amount of time the plant can be
shut down before pressure isolation valve testing will be required from
72 hours to 7 days.
(4) TS SR 4.4.I, 4.4.I.a, 4.4.I.b, 4.4.I.b.1, 4.4.I.b.2, and
4.4.I.b.3, ``Electrical Hydrogen Recombiners.'' Revise the containment
hydrogen recombiner testing surveillance frequency from every 6 months
to every refueling interval. Delete the specific requirement to perform
CHANNEL CALIBRATION of recombiner instruments and control circuits.
Delete the requirement to sequentially perform the resistance to ground
test following the functional test.
(5) TS SR 4.5.A.2.b, ``Containment Spray System.'' Revise the
containment spray system nozzle testing surveillance frequency from
once every 5 years to once every 10 years.
(6) TS SR 4.8.A.1, 4.8.A.2, and Footnote, ``Auxiliary Feedwater
System.'' Revise the testing frequency for the auxiliary feedwater
pumps from intervals of 1 month to semi-quarterly on a staggered test
basis.
(7) BASES 4.8, ``Steam And Power Conversion Systems.'' Revise the
Bases to include testing frequency for the auxiliary feedwater pumps
from intervals of 1 month to semi-quarterly on a staggered test basis.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment[s] will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
Except for hydrogen recombiner changes to conform to Standard
Technical Specifications, the requested changes were extensively
reviewed by the NRC during the preparation of NUREG-1366 and Generic
Letter 93-05. For the sake of clarity each proposed change is
discussed separately in the order appearing in the Prairie Island
Technical Specifications.
A. This Technical Specification amendment removes the
accumulator water level and pressure channel surveillance from the
Technical Specifications and places them into a licensee controlled
test procedure. These changes are consistent with industry
recognition that accumulator instrumentation operability is not
directly related to the capability of the accumulators to perform
their safety function.
Relocating the instrumentation surveillance requirements is an
administrative change which will not affect equipment testing,
availability, or operation. Therefore, it will not have an effect on
the probability or consequences of an accident.
B. This Technical Specification amendment changes control rod
movement from every two weeks to once every quarter. Control rod
movement testing is performed to determine if the control rods are
immovable. Control rods may be electrically stuck due to a problem
in the control rod drive circuitry or mechanically stuck. Electrical
problems with the control rod drive system, in general, do not
prevent insertion of a control rod into [[Page 6306]] the core when
the reactor trip breakers are opened.
NUREG-1366 determined that control rod movement testing is not
effective in determining immovable control rods. Most of the
mechanically immovable control rods are discovered during plant
startup during initial pulling of the rods or during rod drop
testing. Extending the surveillance interval will not affect this
failure discovery method.
The accident analyses assume that the single highest worth rod
is struck while fully withdrawn and will not insert. One immovable
control rod will still bound this accident analysis. For these
reasons, the extension of the surveillance frequency from once every
two weeks to once every quarter will not involve a significant
increase in the probability or consequences of a previously
evaluated accident.
C. This Technical Specification amendment will require Reactor
Coolant Systems Pressure Isolation Valves (PIV) to be surveillance
tested after seven days at cold shutdown instead of after three days
at cold shutdown.
The PIVs are important in preventing over pressurization and
rupture of the Emergency Core Cooling System low pressure piping
which could result in a LOCA [loss-of-coolant accident] that
bypasses containment. Allowable leakage from any PIV is sufficiently
low to ensure early detection of possible in-series check valve
failure. This change will not change the refueling outage
surveillance, nor will it change the required testing to be
performed after maintenance, repair, or replacement. The proposed
level of surveillance is appropriate for these valves.
These valves have had very good operating performance and should
continue to have the same performance record with continuation of
the same maintenance and testing program. Furthermore, these valves
are backed by motor or air-operated valves which have performed
reliably.
For these reasons, the extension of the amount of time from
three days to seven days before pressure isolation valve testing is
required will not result in a significant increase in the
probability or consequences of a previously evaluated accident.
D. This Technical Specification amendment will revise the
containment hydrogen recombiner testing surveillance from every six
months to every refueling interval.
The two independent containment hydrogen recombiners provide
post-accident hydrogen control of the containment atmosphere. The
recombiners are designed to be passive until an accident occurs.
Industry experience and in particular, Prairie Island experience
has demonstrated that this equipment is highly reliable. Since the
recombiners are not required until after an accident, there would
likely be time to effect accessible repairs if the equipment were
not operable.
Relocation of the recombiner calibration is an administrative
change which will not affect recombiner operability. Deletion of
specific testing sequence will not affect the performance of
recombiner testing.
Equipment redundancy, reliability and time for repairs ensures
post-accident control. For these reasons, these changes will not
result in a significant increase in the probability or consequences
of a previously evaluated accident.
E. This Technical Specification amendment will revise the
containment spray system nozzle testing surveillance from once every
five years to once every ten years.
Two independent containment spray systems provide post-accident
cooling of the containment atmosphere and provide a mechanism for
removing iodine from the containment atmosphere. This surveillance
test verifies by air flow test that the spray nozzles are
unobstructed. The extension of the surveillance frequency does not
affect administrative controls that preclude entry of foreign
material into the nozzles.
At Prairie Island the piping headers and nozzles are fabricated
from austenitic stainless steel. There have been no reported in-
service problems noted with spray nozzle testing from plants with
stainless steel headers and nozzles and there is no indication that
the lines would corrode and become obstructed.
For these reasons, this change will not result in a significant
increase in the probability or consequences of a previously
evaluated accident.
F. This Technical Specification amendment will revise the
frequency for testing the Auxiliary Feedwater Pumps (AFWP) from
monthly to semi-quarterly on a STAGGERED TEST BASIS.
Two 100% redundant, diverse pumps provide an emergency source of
feedwater to the steam generators. The Prairie Island AFWPs have
performed reliably. However, frequent testing of the pumps and
associated equipment wears out the equipment resulting in equipment
unavailability. AFWP availability will be increased by semi-
quarterly surveillance testing on a STAGGERED TEST BASIS.
For these reasons, this change will not result in a significant
increase in the probability or consequences of previously evaluated
accident.
Therefore, the probability or consequences of an accident
previously evaluated are not affected by any of the proposed
amendments.
2. The proposed amendment[s] will not create the possibility of
a new or different kind of accident from any accident previously
analyzed.
The extension of facility surveillance intervals as discussed
previously will not result in changes in plant configuration or
operation. The changes in recombiner calibration and testing will
not result in changes in plant configuration or operation.
Therefore, the possibility of a new or different kind of accident
from any accident previously evaluated would not be created.
3. The proposed amendment[s] will not involve a significant
reduction in the margin of safety.
The amendments proposed in this License Amendment Request do not
reduce the ability of any system or component to perform its safety
related function. The basis of NUREG-1366, Generic Letter 93-05, and
the analysis performed in support of this License Amendment Request
is that the reduction in surveillance testing can improve safety by
reducing challenges to plant systems, personnel exposure, and
equipment wear or degradation. The proposed changes to surveillance
frequencies do not change the method of performing any surveillance.
The operation of systems and equipment remains unchanged. Therefore,
a significant reduction in the margin of safety would not be
involved.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and
Trowbridge, 2300 N Street, NW, Washington, DC 20037.
NRC Project Director: John N. Hannon.
Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County,
Minnesota
Date of amendment requests: December 5, 1994.
Description of amendment requests: The proposed amendments would
revise Technical Specification 3.8 to allow containment airlock doors
to remain open during core alterations provided certain conditions are
met. This request is similar to the amendment for Calvert Cliffs
Nuclear Power Plant which the NRC approved on August 30, 1994. In
addition, these amendments would allow containment penetrations to
remain open during core alterations provided certain conditions are
met.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed containment refueling integrity amendments do not
affect the probability of a fuel handling accident, they only deal
with the containment systems.
The containment is provided for the purpose of mitigating the
consequences of postulated accidents. For the fuel handling accident
in containment, the licensing basis analyses, including the NRC
safety [[Page 6307]] evaluation report transmitted February 2, 1982,
assumed that containment was completely abrogated and all
radioactive materials released from the containment refueling pool
are assumed to be released to the outside atmosphere. The requested
amendments to Technical Specification 3.8.A.1.a modify the use of
containment to mitigate the consequences of a fuel handling accident
in containment, however, since instantaneous offsite release of all
fuel handling accident materials released to containment has already
been considered, the probability and consequences of a loss of
containment accident are not increased.
Therefore, the probability or consequences of an accident
previously evaluated are not affected by any of the proposed
amendments.
2. The proposed amendment will not create the possibility of a
new or different kind of accident from any accident previously
analyzed.
The requested amendments to Technical Specification 3.8.A.1.a
modify the use of containment to mitigate the consequences of a fuel
handling accident in containment. There are no new failure modes or
mechanisms associated with the proposed changes, nor do the proposed
changes involve any modification of plant equipment or changes in
plant operational limits. Previous analyses, including the NRC fuel
handling accident safety evaluation for Prairie Island, have already
assumed the containment is abrogated. The proposed license
amendments may affect the release path for fission products released
during a fuel handling accident in containment, but no new or
different kind of accident will result.
Therefore, the possibility of a new or different kind of
accident from any accident previously evaluated would not be
created.
3. The proposed amendment will not involve a significant
reduction in the margin of safety
The margin of safety as defined by the licensing bases fuel
handling accident analyses is not reduced. The previous analyses are
very conservative, assuming all radioactive material released from
[containment] by the fuel handling accident is immediately released
to the outside atmosphere, and bound any changes introduced by these
requested amendments.
Technical Specification 3.8.A.1.a exists to minimize the
consequences of a fuel handling accident in containment. However,
with the current Technical Specification 3.8.A.1.a, there will still
be releases due to the necessity to open the containment airlocks to
evacuate personnel. With implementation of this amendment, the
ability of the closed airlocks to contain the accident releases may
improve.
Some radioactive material could be released through containment
penetrations that are open at the time of the accident. Since it is
not likely that containment will be pressurized by a fuel handling
accident, the releases are expected to be minimal. This amendment
will maintain containment post-fuel handling accident offsite
releases well within the limits of 10CFR100 and the current license
basis releases.
Therefore, a significant reduction in the margin of safety would
not be involved.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and
Trowbridge, 2300 N Street, NW, Washington, DC 20037.
NRC Project Director: John N. Hannon.
Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County,
Minnesota
Date of amendment requests: January 9, 1995.
Description of amendment requests: The proposed amendments would
revise Prairie Island Nuclear Generating Plant Technical Specification
(TS) 4.12, ``Steam Generator Tube Surveillance,'' to incorporate
revised acceptance criteria for steam generator tubes with degradation
in the tubesheet roll expansion region. These criteria for steam
generator tube acceptance were developed by Westinghouse Electric
Corporation and are known as F* (``F-Star'') and L* (``L-Star''). These
criteria would be utilized to avoid unnecessary plugging and sleeving
of steam generator tubes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment[s] will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The supporting technical and safety evaluations of the subject
criterion demonstrate that the presence of the tubesheet will
enhance the tube integrity in the region of the hardroll by
precluding tube deformation beyond its initial expanded outside
diameter. The resistance to both tube rupture and tube collapse is
strengthened by the presence of the tubesheet in that region. The
results of hardrolling of the tube into the tubesheet is an
interference fit between the tube and the tubesheet. Tube rupture
cannot occur because the contact between the tube and tubesheet does
not permit sufficient movement of tube material. The radial preload
developed by the rolling process will secure a postulated separated
tube end within the tubesheet during all plant conditions. In a
similar manner, the tubesheet does not permit sufficient movement of
tube material to permit buckling collapse of the tube during
postulated LOCA loadings.
The F* length of roll expansion is sufficient to preclude tube
pullout from tube degradation located below the F* distance,
regardless of the extent of the tube degradation. The existing
Technical Specification leakage rate requirements and accident
analysis assumptions remain unchanged in the unlikely event that
significant leakage from this region does occur. As noted above,
tube rupture and pullout is not expected for tubes using the F*
criterion. Any leakage out of the tube from within the tubesheet at
any elevation in the tubesheet is fully bounded by the existing
steam generator tube rupture analysis included in the Prairie Island
Plant USAR [Updated Safety Analysis Report]. For plants with partial
depth roll expansion like Prairie Island, a postulated tube
separation within the tube near the top of the roll expansion (with
subsequent limited tube axial displacement) would not be expected to
result in coolant release rates equal to those assumed in the USAR
for a steam generator tube rupture event due to the limited gap
between the tube and tubesheet. The proposed plugging criterion does
not adversely impact any other previously evaluated design basis
accident.
Leakage testing of roll expanded tubes indicates that for roll
lengths approximately equal to the F* distance, any postulated
faulted condition primary to secondary leakage from F* tubes would
be insignificant.
2. The proposed amendment[s] will not create the possibility of
a new or different kind of accident from any accident previously
analyzed.
Implementation of the proposed F* criterion does not introduce
any significant changes to the plant design basis. Use of the
criterion does not provide a mechanism to initiate an accident
outside of the region of the expanded portion of the tube. Any
hypothetical accident as a result of any tube degradation in the
expanded portion of the tube would be bounded by the existing tube
rupture accident analysis. Tube bundle structural integrity will be
maintained. Tube bundle leaktightness will be maintained such that
any postulated accident leakage from F* tubes will be negligible
with regards to offsite doses.
3. The proposed amendment[s] will not involve a significant
reduction in the margin of safety.
The use of the F* criterion has been demonstrated to maintain
the integrity of the tube bundle commensurate with the requirements
of Reg Guide 1.121 [``Bases for Plugging Degraded PWR Steam
Generator Tubes''] (intended for indications in the free span of
tubes) and the primary to secondary pressure boundary under normal
and postulated accident conditions. Acceptable tube degradation for
the F* criterion is any degradation indication in the tubesheet
region, more than the F* distance below the bottom of the transition
between the roll [[Page 6308]] expansion and the unexpanded tube.
The safety factors used in the verification of the strength of the
degraded tube are consistent with the safety factors in the ASME
Boiler and Pressure Vessel Code used in steam generator design. The
F* distance has been verified by testing to be greater than the
length of roll expansion required to preclude both tube pullout and
significant leakage during normal and postulated accident
conditions. Resistance to tube pullout is based upon the primary to
secondary pressure differential as it acts on the surface area of
the tube, which includes the tube wall cross-section, in addition to
the inner diameter based area of the tube. The leak testing
acceptance criteria are based on the primary to secondary leakage
limit in the Technical Specifications and the leakage assumptions
used in the USAR accident analysis.
Implementation of the tubesheet plugging criterion will decrease
the number of tubes which must be taken out of service with tube
plugs or repaired with sleeves. Both plugs and sleeves reduce the
RCS (reactor coolant system) flow margin; thus, implementation of
the F* criterion will maintain the margin of flow that would
otherwise be reduced in the event of increased plugging or sleeving.
Based on the above, it is concluded that the proposed change
does not result in a significant reduction in margin with respect to
plant safety as defined in the USAR or the Technical Specification
Bases.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and
Trowbridge, 2300 N Street, NW, Washington, DC 20037.
NRC Project Director: John N. Hannon.
Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County,
Minnesota
Date of amendment requests: January 13, 1995.
Description of amendment requests: The proposed amendments would
revise Prairie Island Nuclear Generating Plant Technical Specification
4.4.D.1 to change the interval for the performance of the Residual Heat
Removal (RHR) System leakage test from once every 12 months to perform
the test during each refueling shutdown.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed amendment[s] will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed changes to the RHR system leakage test interval
only involve the leak-tightness of the RHR system for postaccident
operation. As such, the proposed changes will have no impact on the
probability of an accident previously evaluated.
The extension of the RHR system leakage test interval could
increase the possibility of undetected RHR system leakage outside
the containment during post accident conditions. However, the
possible consequences of leakage from the RHR system outside
containment are minor relative to those of the design basis
accident. Therefore, because leakage from the RHR system has a minor
effect on offsite dose, and since previous testing on a 12 month
interval has not found significant RHR system leakage, the extension
of the test interval to refueling is not expected to significantly
impact the offsite dose consequences of an accident. In addition, it
is probable that RHR system leakage would be identified during the
normal quarterly functional testing and inspection of the RHR
system.
Therefore, for the reasons discussed above, the proposed changes
will not significantly affect the probability or consequences of an
accident previously evaluated.
2. The proposed amendment[s] will not create the possibility of
a new or different kind of accident from any accident previously
analyzed.
There are no new failure modes or mechanisms associated with the
proposed changes. The proposed changes do not involve any
modification of the plant equipment or any changes in operational
limits. The proposed changes only modify the interval for the
performance of the RHR system leakage test. The performance of the
RHR system leakage test on a refueling basis instead of every 12
months cannot create a new or different kind of accident.
Therefore, for the reasons discussed above, the proposed changes
do not create the possibility of a new or different kind of accident
from any previously evaluated, and the accident analyses presented
in the Updated Safety Analysis Report [USAR] will remain bounding.
3. The proposed amendment[s] will not involve a significant
reduction in the margin of safety.
The performance of the RHR system leakage test at power is more
complex than performing the test during refueling shutdown. It is
preferable, from an RHR system reliability and plant safety
standpoint, to perform the test during refueling shutdown when the
RHR system is already operating and when no changes to the RHR
system configuration are required. Any possible increase in the risk
to the public health and safety incurred by extending the RHR leak
test interval from 12 months to refueling shutdown will be off-set
by the reduction in risk obtained by not performing the RHR system
leakage test during power operation.
The extension of the test interval would mean that possible RHR
leakage could exist undetected for a longer period than allowed by
the current Technical Specifications. However, the possible
consequences of leakage from the RHR system outside containment are
minor relative to those of the design basis accident. In addition,
it is probable that RHR system leakage would be identified during
the normal quarterly functional testing and inspection of the RHR
system.
Based on the above, it is concluded that the proposed change
does not result in a significant reduction in margin with respect to
plant safety as defined in the USAR or the Technical Specification
Bases.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and
Trowbridge, 2300 N Street, NW, Washington, DC 20037.
NRC Project Director: John N. Hannon.
Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311,
Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New
Jersey
Date of amendment request: December 23, 1994.
Description of amendment request: The proposed amendment to the
Technical Specifications revises the surveillance requirement to
perform a visual inspection of containment areas affected by
containment entry when containment integrity is established. It is
consistent with Item 7.5 of Generic Letter 93-05, ``Line-Item Technical
Specifications Improvements to Reduce Surveillance Requirements for
Testing During Power Operation.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does not involve a significant increase in the probability or
consequences of an accident previously evaluated. [[Page 6309]]
The proposed change does not alter the assumptions, design
parameters or results of Updated Final Safety Analysis Report
(UFSAR) accidents analyzed. The proposed change does not involve a
hardware change, a change to the operation of any systems or
components, or a change to any existing structures. The proposed
change leads to a reduction in radiation exposure to plant personnel
and the elimination of an unnecessary burden on plant staff. The
revised visual inspection practice will not increase the probability
or consequences of an accident previously evaluated.
2. Does not create the possibility of a new or different kind of
accident from any previously evaluated.
The proposed change does not modify equipment, affect system
design bases or operability. This change does not alter parameters
utilized in the analyzed accident scenarios. The proposed change in
surveillance frequency is consistent with the guidance provided in
GL 93-05. The performance of a visual inspection of containment
areas affected by multiple containment entries on a daily bases
[basis] and at the completion of the final entry when containment
integrity is established will not create the possibility of a new or
different kind of accident from those previously evaluated.
3. Does not involve a significant reduction in a margin of
safety.
The proposed change only involves a decrease in surveillance
frequency when multiple entries are made in a single day and does
not alter the performance of the surveillance itself. System
equipment and operation remains unchanged. Operability and
reliability is still maintained by the required inspection. The
adaptation of the proposed surveillance frequency does not involve a
significant reduction in the margins of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Salem Free Public Library, 112
West Broadway, Salem, New Jersey 08079.
Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and
Strawn, 1400 L Street, NW, Washington, DC 20005-3502.
NRC Project Director: John F. Stolz.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee.
Date of amendment request: December 16, 1994 (TS 94-06).
Description of amendment request: The proposed change would revise
the auxiliary feedwater system technical specifications and associated
Bases by incorporating the Westinghouse Standard Technical
Specification limits and format, extending the limiting condition for
operation to Mode 4, relaxing the achievement of hot shutdown from 6
hours to 12 hours, relaxing the verification of valve position
surveillance frequency from 7 days to 31 days, and verifying the
position of automatic valves every 31 days in lieu of valve
manipulation.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
TVA has evaluated the proposed technical specification (TS)
change and has determined that it does not represent a significant
hazards consideration based on criteria established in 10 CFR
50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance
with the proposed amendment will not:
1. Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The proposed TS change replaces SQN's auxiliary feedwater (AFW)
system specification and the associated bases section with improved
requirements that are modeled after the Westinghouse Standard
(NUREG-1431) Technical Specification (STS). The proposed change is
consistent with the STS for ensuring that three trains of AFW remain
operable in Modes 1, 2, and 3. In addition, the proposed change
provides a TS improvement by extending the limiting condition for
operation (LCO) applicability to Mode 4. This LCO requirement for
Mode 4 ensures that at least one motor-driven AFW pump remains
operable when steam generators are being used for decay heat
removal. The proposed 72 hour allowed outage time (for one
inoperable train of AFW) is consistent with the STS and remains
unchanged from SQN's current allowed outage time. One proposed
change to relax shutdown requirements from 6 hours to 12 hours for
achieving hot shutdown is considered to be acceptable. This
relaxation is based on shutdown times contained in the STS and the
operating experience to reach thus condition from full power in an
orderly manner without challenging plant systems. The proposed
surveillance requirements (SRs) provide test frequencies that are
consistent with the STS and are based on operating experience and
the design reliability of the equipment. The proposed relaxation in
surveillance frequency from 7 days to 31 days for verifying valve
position in the AFW flow path is considered acceptable based on
existing procedural controls for valve configuration. The proposed
change to include a STS SR for verifying automatic valves in the
flow path are in their correct position every 31 days (in lieu of
valve manipulation) is considered acceptable based on existing
surveillance that verify proper actuation of SQN's automatic AFW
valves.
The proposed changes provide TS improvements for SQN's AFW
system that ensure the system operates within the bounds of SQN's
AFW accident analysis as contained in the Final Safety Analysis
Report (FSAR). This change does not involve a physical modification
to SQN's AFW system. Accordingly, the proposed changes do not
involve an increase in the probability or consequences of an
accident previously evaluated.
2. Create the possibility of a new or different kind of accident
from any previously analyzed.
The proposed TS change incorporates requirements that bound the
limiting design-basis accidents (DBAs) evaluated in SQN's FSAR. The
TS bases have been revised to reflect the limiting DBAs and provide
clarification with regard to the assumptions used in SQN's AFW
accident analysis. No new event initiator has been created, not
[sic] has any hardware been changed. This change does not involve a
physical change to SQN's AFW system or any other system. Therefore,
the proposed change will not create the possibility of a new or
different kind of accident from any previously analyzed.
3. Involve a significant reduction in a margin of safety.
TVA's proposed change replaces SQN's AFW system TS requirements
with TS requirements adopted from the Westinghouse STS. Because the
overall similarity in the requirements between SQN's current AFW
specification and the STS version, the TS requirements remain
essentially unchanged. The proposed 72-hour allowed outage time (for
one inoperable train of AFW) is consistent with the STS and remains
unchanged from SQN's current allowed outage time. One proposed
change to relax shutdown requirements from 6 hours to 12 hours for
achieving hot shutdown is considered to be acceptable. This
relaxation is based on shutdown times contained in the STS and the
operating experience to reach this condition from full power in an
orderly manner without challenging plant systems. The proposed SRs
provide test frequencies that are consistent with the STS and are
based on operating experience and the design reliability of the
equipment. The proposed relaxation in surveillance frequency from 7
days to 31 days for verifying valve position in the AFW flow path is
considered acceptable based on existing procedural controls for
valve configuration. The proposed relaxation in surveillance
frequency from 7 days to 31 days for verifying valve position in the
AFW flow path is considered acceptable based on existing procedural
controls for valve configuration. The proposed change to include a
STS SR for verifying automatic valves in the flow path are in their
correct position every 31 days (in lieu of valve manipulation) is
considered acceptable based on other existing surveillances that
verify proper actuation of SQN's automatic AFW valves.
The proposed changes provide TS improvements for SQN's AFW
System that ensure the system operates within the bounds of SQN's
AFW accident analysis as contained in the FSAR. This change does not
[[Page 6310]] involve a physical modification to SQN AFW system.
Accordingly, the margin of safety has not been reduced.
The NRC has reviewed the licensee's analysis and, based on this
review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Chattanooga-Hamilton County
Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902.
NRC Project Director: Frederick J. Hebdon.
The Cleveland Electric Illuminating Company, Centerior Service Company,
Duquesne Light Company, Ohio Edison Company, Pennsylvania Power
Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power
Plant, Unit No. 1, Lake County, Ohio
Date of amendment request: December 16, 1994.
Description of amendment request: The proposed license amendment
would revise Technical Specification 6.3, ``Unit Staff
Qualifications.'' Currently, the Technical Specifications require that
the Operations Manager obtain a senior reactor operator (SRO) license
by August 1995. A change is proposed to relieve the requirement for the
Operations Manager to hold a Perry Nuclear Power Plant (PNPP) SRO
license if an Operations section middle manager holds a PNPP SRO
license.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The proposed change affects an administrative control, which was
based on the guidance of ANSI N18.1-1971, ``Selection and Training
of Nuclear Power Plant Personnel.'' ANSI N18.1-1971 recommended that
the Operations Manager hold a senior reactor operator (SRO) license.
The current guidance in Section 4.2.2 of ANSI/ANS-3.1-1993,
``American National Standard for Selection, Qualification, and
Testing of Personnel for Nuclear Power Plants'' recommends, as one
alternative, that the Operations Manager have plant operational
knowledge consistent with the requirements of the Operations
Manager's position, providing an Operations middle manager holds an
SRO license. This individual (currently designated as the Operations
Superintendent) would be required to meet the criteria for, and
would have responsibilities as recommended in, ANSI/ANS-3.1-1993 for
the Operations Middle Manager position. The proposed change is
consistent with the recommendations of ANSI/ANS-3.1-1993.
The proposed change does not alter the design of any system,
structure or component, nor does it change the way plant systems are
operated. It does not reduce the knowledge, qualifications, or
skills of licensed operators, and does not affect the way the
Operations Section is managed by the Operations Manager. The
Operations Manager will continue to maintain the effective
performance of section personnel and ensure the plant is operated
safely and in accordance with the requirements of the operating
license. Additionally, the control room operators will continue to
be supervised by the licensed senior operators such as the Unit
Supervisors and the Shift Supervisors. For those areas of knowledge
that require an SRO license, the Operations Superintendent will
provide the appropriate technical guidance to the control room
staff.
In summary, the proposed change does not affect the ability of
the Operations Manager to provide the plant oversight required of
the position. Thus, it does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
The proposed change to Technical Specification 6.3.1 does not
affect the design or function of any plant system, structure, or
component, nor does it change the way plant systems are operated. It
does not affect the performance of NRC licensed operators. Operation
of the plant in conformance with the Technical Specifications and
other license requirements will continue to be supervised by
personnel who hold an NRC SRO license. The proposed change to
Technical Specifications 6.3.1 ensures that either the Operations
Manager or Operations Superintendent will be a knowledgeable and
qualified individual by requiring one of the individuals to hold an
SRO license for PNPP. Based on the above, the proposed change does
not create the possibility of a new or different kind of accident
from any previously evaluated.
3. The proposed change does not result in a significant
reduction in the margin of safety.
The proposed change involves an administrative control which is
not related to the margin of safety as defined in the Technical
Specifications. The proposed change provides an alternative which
ensures that the level of knowledge and experience required of an
individual who fills the Operations Manager position is acceptable.
The proposed change does not affect the conservative manner in which
the plant is operated. The control room operators will continue to
be supervised by personnel who hold an SRO license. Thus, the
proposed change does not involve a significant reduction in a margin
of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Perry Public Library, 3753
Main Street, Perry, Ohio 44081.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Project Director: Leif J. Norrholm.
The Cleveland Electric Illuminating Company, Centerior Service Company,
Duquesne Light Company, Ohio Edison Company, Pennsylvania Power
Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power
Plant, Unit No. 1, Lake County, Ohio
Date of amendment request: December 21, 1994.
Description of amendment request: The proposed license amendment
would revise Technical Specification 3/4.3.7.7, ``Traversing In-Core
Probe System,'' and its Bases to allow the use of substitute data
generated from the process computer, normalized with available
operating measurements, to replace data from inoperable local power
range monitor (LPRM) strings for up to 10 LPRM strings.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The TIP [traversing in-core probe] system is not used to prevent
or mitigate the consequences of any previously analyzed accident or
transient. No assumptions are made in any accident analysis relative
to the operation of the TIP system. No other safety related system
is affected by this change.
The use of substitute values from calculations performed by the
on-line computer core monitoring system does not affect the
consequences of plant transients previously evaluated in the USAR
[Updated Safety Analysis Report] because the total core TIP reading
(nodal power) uncertainty remains less than 8.7%. Thus, the MCPR
[minimum critical power ratio] safety limit is not affected.
2. The proposed change does not create the possibility of a new
or different kind of [[Page 6311]] accident from any accident
previously evaluated.
The proposed change does not involve the installation of any new
equipment or the modification of any equipment designed to prevent
or mitigate the consequences of accidents or transients. Therefore,
the change has no effect on any accident initiator, and no new or
different type of accidents are postulated to occur.
3. The proposed change does not result in a significant
reduction in the margin of safety.
The total core TIP reading uncertainties will remain within the
assumptions of the licensing basis; thus, the margin of safety to
the MCPR safety limits is not reduced. The ability of the computer
to accurately represent nodal powers in the reactor core is not
compromised. The ability of the computer to accurately predict the
LHGR [linear heat generation rate], APLHGR [average planar linear
heat generation rate], MCPR, and its ability to provide for LPRM
calibration, are not compromised. Therefore, the margin of safety is
not significantly reduced.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Perry Public Library, 3753
Main Street, Perry, Ohio 44081.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Project Director: Leif J. Norrholm.
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam
Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: December 6, 1994.
Brief description of amendments: The proposed amendment would
revise Technical Specifications to allow appropriate remedial action
for high particulate levels in the diesel generator fuel oil inventory
and other out-of-limit properties in new diesel generator fuel oil that
has been added to the existing diesel generator fuel oil storage
inventory.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed changes do not involve a significant increase in
the probability or consequences of an accident previously evaluated.
The proposed changes allow 7 days to correct particulate
contamination in the stored fuel oil for the diesel generators and
30 days to confirm or restore the adequacy of the stored fuel oil if
certain properties of new fuel that has been added to the fuel oil
storage inventory have been discovered to exceed the specified
values. These changes do not affect plant operations and the only
equipment affected are the diesel generators. The ability of the
diesel generators to provide electrical power when needed is
directly dependent upon, in part, having fuel oil of adequate
quality. The only accident which is potentially initiated by a
diesel generator failure is the station blackout event. The
mitigation of many accidents is dependent upon the availability of
at least one train of electrical power from an emergency diesel
generator (EDG). With the proposed changes, the fuel oil should
continue to have sufficient quality to assure the operability of the
diesel generators until the particulate and other properties are
returned to within limits. This is due in part to the existing fuel
oil quality requirements that are more stringent than the vendor
requires for the EDG to operate and the system of filters installed
to insure good quality fuel actually reaches the EDG. Even though
the margin provided in the quality of the fuel oil may be affected
(see the response to question 3 below), adequate fuel oil quality is
being maintained to assure the operability of the diesel generators
and therefore, these changes do not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. The proposed changes do not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
There are no hardware changes and no changes in system
operations involved. These changes only affect the quality of the
stored fuel oil for the diesel generators. The availability of a
diesel generator has been addressed by the CPSES [Comanche Peak
Steam Electric Station] design and in particular by the analysis of
the station blackout event. These changes do not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. The proposed changes do not involve a significant reduction
in a margin of safety.
The margin of safety of interest for these changes is the
quality of the stored fuel oil for the diesel generators as compared
to minimum quality which will support the diesel generators ability
to supply electrical power when needed. Particulate contamination
increases slowly over a period of time due to the chemical breakdown
of the fuel oil (or its additives or the surfaces on the tanks
themselves) or due to the introduction of foreign material during
refueling activities. When considered with the fact that the
existing limitation of 10 mg/L was developed for engines which
require much cleaner fuel oil (aircraft engines) and that the CPSES
diesel engines have in line duplex fuel oil filters which can be
switched while the engine is operating, the 7 days which are being
provided to restore the particulate levels do not involve a
significant reduction in the margin of safety. The levels of
particulate are expected to not exceed the specified value by a
significant amount and the specified value is already quite
conservative. Seven days is a reasonable time period in which to
restore the parameter but is short enough to ensure that the
contamination values do not exceed the vendors recommended fuel oil
tolerances required for the EDGs to run. In a similar manner, the
properties of the new fuel oil that has been added to the fuel oil
storage inventory are not expected to deviate significantly from the
allowed values. The testing for gravity, viscosity, flash point,
clarity, water and sediment prior to adding the new fuel oil
provides adequate assurance that the stored fuel oil will be of
sufficient quality to support diesel generator operation. The
quality of the stored fuel oil is further protected from problems
being introduced by new fuel oil that has been added to the fuel oil
storage inventory by the fact that the new fuel oil is generally
diluted by a factor of four or more when it is added to the storage
tanks by the fuel oil that is already in the tanks. Allowing 30 days
to confirm or restore the properties of the stored fuel oil when a
sample of new fuel that has been added to the fuel oil storage
inventory has properties which exceed their specified values does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, Texas 76019.
Attorney for licensee: George L. Edgar, Esq., Newman and
Holtzinger, 1615 L Street, N.W., Suite 1000, Washington, D.C. 20036.
NRC Project Director: William D. Beckner.
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam
Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: December 7, 1994.
Brief description of amendments: The proposed amendment to the
technical specifications (TSs) would: (1) revise the Comanche Peak
Steam Electric Station (CPSES), Technical Specification Limiting
Condition for Operation (LCO) for the main steam isolation valves
(MSIVs) to increase the allowed outage time (AOT) in Mode 1; (2)
relocate the MSIVs full closure time requirement to a program
administratively controlled by the TS; and (3) revise the associated
Bases to [[Page 6312]] adopt the expanded Bases format adding
information specific to CPSES.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
The proposed changes are to (1) revise the CPSES Technical
Specification Limiting Condition for Operation (LCO) for the MSIVs
to increase the Allowed Outage Time (AOT) from 4 hours to 8 hours in
Mode 1; (2) modify the Mode 2 and 3 Action Statement to better
reflect the safety significance of these valves by requiring that
the valves be closed within 8 hours and verified at least every 7
days; (3) relocate the MSIVs full closure time requirement to a
program administratively controlled by the TS; and (4) revise the
associated Bases to adopt the expanded Bases format adding
information specific to CPSES.
The revision of the CPSES Technical Specification Limiting
Condition For Operation (LCO) for the MSIVs to increase the Allowed
Outage Time (AOT) from 4 hours to 8 hours in Mode 1 only affects the
time that a condition can exist and as such does not affect any of
the conditions that could initiate an accident; therefore the
probability of an accident is not affected. Likewise, no new
conditions are created that would affect the analyses of any
accident; therefore the consequences of the accidents postulated for
CPSES are not affected.
Modifying the Mode 2 and 3 Action Statement to better reflect
the safety significance of these valves by requiring that the valves
be closed within 8 hours and verified at least every 7 days provides
clarity and adds a new verification requirement. Again no new plant
conditions are established, time limits and verification
requirements are merely being established; therefore, no accident
initiators are affected and there is no impact on the probability of
any accident. Likewise no conditions are being altered which affect
the analyses of any accidents which are postulated at CPSES and thus
the consequences of those accidents are unaffected.
Relocating the MSIVs full closure time requirement to a program
administratively controlled by the TS is an administrative change
only. It has no impact on actual plant operation and thus there is
no impact on the probability of any accident or on the consequences
of any accident.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
None of the changes in this request affect plant design or create
new operating configurations. The only things affected are the times
that certain conditions are allowed, how soon actions need be
performed, how often to verify conditions and the administrative
location of certain requirements. These items do not create the
possibility of a new type or different kind of accident.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
The Technical Specifications LCOs ensure that the assumptions of
the safety analyses are preserved. There are no substantive changes
to the LCO; therefore, the safety analyses are unaffected and there
is no affect on the margin of safety.
Revising the CPSES Technical Specification Limiting Condition
For Operation (LCO) for the MSIVs to increase the Allowed Outage
Time (AOT) from 4 hours to 8 hours in Mode 1 allows the unit to
operate with an inoperable MSIV for a longer period of time.
Although the unavailability of equipment required to mitigate or
assess the consequence of an accident is increased, a more
reasonable completion time is provided to diagnose the problem,
mobilize the corrective action, obtain administrative clearances,
complete the maintenance, restore the valve to an operable
condition, and perform post-maintenance verification, where
appropriate. The additional time would reduce the probability of
unnecessary plant transients and plant shutdowns, thus improving
plant safety and increasing plant availability, while a qualitative
assessment has concluded that the impact on Core Damage Frequency is
negligible. TU Electric has concluded based on the discussion above
that there is no significant impact on the overall margin of safety
due to this change.
Modifying the Mode 2 and 3 Action Statement to better reflect
the safety significance of these valves by requiring that the valves
be closed within 8 hours and verified at least every 7 days is
primarily a clarification and a new verification requirement.
Specifying that an inoperable valve be closed within 8 hours makes
the requirement specific where no time limit was provided before.
The 8 hours specified is the same as is allowed in Mode 1 which was
qualitatively assessed as noted above and thus is a logical
limitation. The new requirement to verify the valves closed on a
periodic basis will increase assurance that the valves remain closed
and will thus enhance the margin of safety. Overall, TU Electric
concludes that these Mode 2 and 3 changes do not significantly
affect the margin of safety.
Relocating the MSIVs full closure time requirement to a program
administratively controlled by the TS is an administrative change
only. There is no impact on the margin of safety.
Revising the associated Bases to adopt the expanded Bases format
adding information specific to CPSES enhances the useability of the
Technical Specification. Overall, this is considered an improvement
which will benefit both the operators and support personnel. There
is no significant impact on the margin of safety and if there is an
impact, it improves the margin by providing easy access to support
information.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, Texas 76019.
Attorney for licensee: George L. Edgar, Esq., Newman and
Holtzinger, 1615 L Street, N.W., Suite 1000, Washington, D.C. 20036.
NRC Project Director: William D. Beckner.
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam
Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: December 19, 1994.
Brief description of amendments: The proposed changes to the
Technical Specification Action Statements of Tables 3.3-1 and 3.3-2
would allow testing of the reactor protective system (RPS) and the
engineered safety features actuation system (ESFAS) with the channel
under test in bypass.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
(1) Do the proposed changes involve a significant increase in
the probability or consequences of an accident previously evaluated?
The proposed changes will revise those Action Statements which
limit the use of bypass while testing for Reactor Protection System
(RPS) and Engineered Safety Feature Actuation System (ESFAS)
functions. The Actions Statements concern testing with a channel
inoperable and will be revised to allow testing with either the
inoperable channel or the channel being tested (but not both) placed
in bypass.
Testing in a bypass condition when all channels are operable
will not introduce new operating configurations. The number [of]
available channels with one channel in bypass for testing will
remain the same as the minimum number of channels and is the same as
the number of channels available when testing in trip. The number of
channels to trip will be unchanged when testing in bypass while the
number of channels to trip is reduced to one when testing in trip.
Although there may be a sight [slight] increase in possibility that
the failure of a channel could prevent the actuation of a function
(because testing in bypass could result in two-out-of-two logic
while testing in trip would have resulted in one-out-of-two logic),
testing in bypass will reduce the vulnerability to inadvertent
actuation of a function while maintaining the normal channels to
trip and the minimum channels [[Page 6313]] operable requirements
per the current technical specifications. Overall TU Electric
concludes (and WCAP-10271 with its associate SER from the NRC
supports) that testing in bypass when all channel [s] are operable
does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
Testing in bypass with one channel inoperable will not introduce
new configurations. The current Actions Statements for ESFAS already
allow testing in bypass if one channel is inoperable. Under the
current Technical Specifications for an RPS function, an inoperable
channel is placed in bypass (via leads and jumpers) while
surveillance testing another channel (the channel under test is
placed in trip). Under the proposed changes, either the inoperable
channel or the channel being tested may be bypassed.
In either case, the result is one channel in bypass and the
other in trip, which leaves one-out-of-two operable channels to
initiate the protective function (if the initial logic was two-out-
of-four) or one-out-of-one operable channels to initiate the
protective function (if the initial logic was two-out-of-three).
Thus, testing in bypass with one channel inoperable does not involve
a significant increase in the probability or consequences of an
accident previously evaluated.
The proposed technical specification changes will also allow
certain ESFAS functions to be tested with an inoperable channel in
bypass and the channel being tested in trip. The current technical
specifications require that the inoperable channel be in trip and
that the channel being tested be in bypass. Per the same logic
provided above on testing in bypass with an inoperable channel, this
change has no impact on the capability of the system to respond to
plant conditions and does increase the potential for inadvertent
actuation of a function.
In summary, the proposed changes to the technical specifications
and testing in bypass do not increase the probability or
consequences of an accident previously evaluated.
(2) Do the proposed changes create the possibility of a new or
different type of accident from any accident previously evaluated?
No new operating configurations and no new failure modes are
being introduced by testing in bypass or by the proposed technical
specification changes; therefore, no new or different type of
accident from any accident previously evaluated is being created.
(3) Do the proposed changes involve a significant reduction in
the margin of safety?
Testing in bypass does not affect accident configurations,
sequences, or response scenarios as modeled in the safety analyses.
Testing or maintenance in a bypass configuration does not cause any
design or analysis acceptance criteria to be exceeded, nor does it
affect the integrity of the fission product barriers. The severity
of any accident previously evaluated is not increased. Bypass
testing does not affect the functional integrity of the Reactor
Protection System (RPS) or the Engineered Safety Features Actuation
System (ESFAS). Bypass testing and the proposed technical
specification changes do not involve a significant reduction in the
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, Texas 76019.
Attorney for licensee: George L. Edgar, Esq., Newman and
Holtzinger, 1615 L Street, N.W., Suite 1000, Washington, D.C. 20036.
NRC Project Director: William D. Beckner.
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam
Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: December 30, 1994
Brief description of amendments: The proposed amendments would
revise the technical specification for fuel storage to authorize use of
the high density fuel storage racks, to increase the spent fuel storage
capacity, and to adopt the wording, content, and format of the Improved
Standard Technical Specifications.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequence of an accident previously evaluated?
This proposed license amendment includes changes which clarify
the Technical Specifications, identify existing licensing basis
criteria, revise the wording and format to be consistent with the
Improved Standard Technical Specifications (NUREG-1431), and provide
the criteria for acceptable fuel storage in high density racks. The
clarification and the revised wording and format are purely
administrative changes and have no impact on the probability or
consequences of an accident. The criteria for acceptable fuel
storage in the high density racks are discussed below.
The high density racks differ from the low density racks in that
the center to center storage cell spacing is decreased from a
nominal 16 inches to a nominal 9 inches and the high density racks
are free standing whereas the low density racks are bolted to the
pool. The allowed storage pattern in the high density racks results
in a nominal 12.7 inch center to center spacing (measured
diagonally) with a two out of four storage pattern (high density (2/
4)). Administrative controls are used to maintain the specified
storage patterns and to assure storage of a fuel assembly in a
proper location based on initial U-235 enrichment and burnup. The
increased storage capacity results in added weight in the pools and
additional heat loads.
The only potential impact on the probability of an accident
concerns the potential insertion of a fuel assembly in an incorrect
location in the high density racks. TU Electric has used
administrative controls to move fuel assemblies from location to
location since the initial receipt of fuel on site. Through receipt
of fuel for two initial core loads and four refueling outages (each
of which includes a complete core offload), TU Electric has not
inserted a fuel assembly into an improper location. This record
demonstrates the adequacy of the administrative controls in place
and confirms that the use of such administrative controls will not
involve a significant increase in the probability of an accident
previously evaluated.
The consequences of all of these changes have been assessed and
the current acceptance criteria in the licensing basis of CPSES will
continue to be met. The nuclear criticality, thermal-hydraulic,
mechanical, material and structural designs will accommodate these
changes. Potentially affected analyses, including a dropped spent
fuel assembly, a loss of spent fuel pool cooling, a seismic event,
and a fuel assembly placed in a location other than a prescribed
location, continue to satisfy the CPSES licensing basis acceptance
criteria. The analysis methods used by TU Electric are consistent
with methods used by TU Electric in the past or methods used
elsewhere in the industry and accepted by the NRC.
Based on the acceptability of the methodology used and
compliance with the current CPSES licensing basis, TU Electric
concludes that the use of the high density racks and the increase in
storage capacity do not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
The administrative changes to the Technical Specifications have
no impact on plant hardware or operations and therefore cannot
create a new or different kind of an accident.
The spacing changes between fuel assemblies, the administrative
controls, the storage limitations, and the increased storage
capacity do not generate new failure modes that could create a new
or different kind of an accident. The change from bolted low density
racks to free standing high density racks will not create the
possibility of a new or different kind of an accident. Free standing
racks have been commonly used at nuclear power plants to provide for
high density storage of spent fuel, and their use [[Page 6314]] does
not entail any unproven or unusual design or technology. In this
regard, a number of plants have previously changed from bolted or
restrained racks to free standing racks, including Millstone 1
(amendment dated November 27, 1989) and San Onofre 2 and 3
(amendment dated May 1, 1990), and such changes have not been
classified as involving a significant hazards consideration.
Furthermore, CPSES is not located in an area subject to severe
seismic events. A seismic event at CPSES would result in little
movement of the free standing racks and would not cause the high
density racks to collide with each other or the spent fuel pool
walls. Therefore, use of the free standing high density racks would
not create the possibility of a new or different kind of an
accident.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
The proposed administrative changes to the Technical
Specifications have no impact on any acceptance criteria, plant
operations or the actual failure of any systems, components or
structure; therefore these administrative changes have no impact on
the margin of safety.
The NRC guidance [Nuclear Regulatory Commission, Letter to all
Power Reactor Licensees, from B. K. Grimes, April 14, 1978, ``OT
Position for Review and Acceptance of Spent Fuel Storage and
Handling Applications,'' as amended by the NRC Letter dated January
18, 1979] has established that an evaluation of margin of safety
should address the following areas:
(1) Nuclear criticality considerations.
(2) Thermal-Hydraulic considerations.
(3) Mechanical, material and structural consideration.
The established acceptance criterion for criticality is that the
neutron multiplication factor in the spent fuel pool storage racks
shall be less than or equal to 0.95, including uncertainties, under
all conditions. The keff for the high density racks for CPSES
is always less than 0.95, including uncertainties at a 95/95
probability confidence level. Because the existing acceptance
criterion is shown to be satisfied, the high density racks do not
involve a significant reduction in the margin of safety with respect
to criticality considerations.
The thermal-hydraulic evaluation demonstrates that the
temperature margin of safety will be maintained. Re-evaluation of
the spent fuel pool cooling system for the increased heat loads
shows, with minor modifications, that the spent fuel cooling system
will maintain the abnormal maximum temperature of the spent fuel
pool water within the limits of the existing licensing basis (i.e.,
below 212 deg.F). Additionally, it shows that, with minor
modifications, the normal maximum temperature will be within the
existing design basis temperatures for the high density racks,
liner, structure, and cooling system and will not have any
significant impact on the spent fuel pool demineralizers. Thus, the
existing licensing basis remains valid, and there is no significant
reduction in the margin of safety for the thermal-hydraulic design
or spent fuel cooling.
The main safety function of the spent fuel pool and the high
density racks is to maintain the spent fuel assemblies in a safe
configuration through normal and abnormal operating conditions. The
design basis floor responses of the Fuel Building were confirmed to
be adequate and conservative and the floor loading will not exceed
the capacity of the Fuel Building. The high density rack materials
used are compatible with the spent fuel pool and the spent fuel
assemblies. The structural considerations of the high density racks
maintain margin of safety against tilting and deflection or
movement, such that the high density racks do not impact each other
or the pool walls, damage spent fuel assemblies, or cause
criticality concerns. Thus, the margin of safety with respect to
mechanical, material and structural considerations are not
significantly reduced by the use of the high density racks.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, Texas 76019.
Attorney for licensee: George L. Edgar, Esq., Newman and
Holtzinger, 1615 L Street, N.W., Suite 1000, Washington, DC 20036.
NRC Project Director: William D. Beckner.
Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: December 9, 1994.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) 4.3.2.2, 4.7.1.2.1, and the Bases
for Specification 3/4.7.1.2. The changes would decrease the frequency
of testing auxiliary feedwater pumps, provide consistent testing
requirements for the steam turbine-driven auxiliary feedwater pump, and
clarify performance parameters in the Bases.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
The proposed revision does not involve a significant hazards
consideration because operation of Callaway Plant with this change
would not:
(1) Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The Callaway Final Safety Analysis Report has been reviewed and
been found to be unaffected by these proposed changes. The changes
proposed by this Technical Specification amendment do not affect the
performance parameters of the Auxiliary Feedwater System (AFWS). The
changes proposed involve a decrease in the frequency of pump testing
from once per 31 days to once per 92 days as recommended by NRC
Generic Letter 93-05 and reflected in NUREG-1431 (T/S 4.7.1.2.1.a).
This change will decrease the out-of-service time of the AFWS due to
testing. This change will also decrease the number of component
manipulations performed on the system and will therefore decrease
the probability of a restoration error rendering the system
incapable of performing its intended function.
The pumps will be required to meet the same acceptance criteria
and will continue to be monitored as required by ASME Section XI. As
stated earlier, the overall effect is a slight decrease in the CDF
for Callaway. These proposed changes will also eliminate an
inconsistency among Specifications 4.7.1.2.1.b.2 and 4.3.2.2 and
Specification 4.7.1.2.1.a.2 regarding an exception to Specification
4.0.4 for entry into Mode 3 for the TDAFP. The methodology and
acceptance criteria of surveillance testing will not be changed. The
ability of the AFWS to perform its intended function during accident
conditions will continue to be demonstrated via surveillance
testing. The proposed changes to the Technical Specifications do not
affect any accident initiators for any accident evaluated in the
Final Safety Analysis Report (FSAR). The Bases changes are
corrections to errors which have no effect on any accident
initiators nor equipment failure modes.
(2) Create the possibility of a new or different kind of
accident from any previously evaluated.
The proposed Technical Specification changes do not modify any
equipment nor create any potential accident initiators. The proposed
change herein of potential interest is the exception to
Specification 4.0.4 for entry into Mode 3 for TDAFP response time
testing and auto-start testing. This allowance is already recognized
via Specification 4.7.1.2.1.a.2 and NUREG-1431, Standard Technical
Specifications-Westinghouse Plants.
(3) Involve a significant reduction in a margin of safety.
The Bases for Specification 3/4.7.1.2 are to be clarified to
correctly state the design flow and pressure parameters for the
AFWS. No plant design changes are involved in any of the proposed
changes and the method and manner of plant operation remain the
same. The specific surveillance test methodology and acceptance
criteria remain unchanged.
As discussed above, the proposed change does not involve a
significant increase in the probability or consequences of an
accident previously evaluated or create the possibility of a new or
different kind of accident from any previously evaluated. These
changes do not result in a significant reduction in a margin of
safety. Therefore, it has been determined that the proposed changes
do not involve a significant hazards consideration.
[[Page 6315]] The NRC staff has reviewed the licensee's analysis
and, based on this review, it appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to
determine that the amendment request involves no significant hazards
consideration.
Local Public Document Room location: Callaway County Public
Library, 710 Court Street, Fulton, Missouri 65251.
Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts
& Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
NRC Project Director: Leif J. Norrholm.
Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: December 9, 1994, as supplemented on
December 22, 1994.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) Surveillance Requirement
4.8.1.1.2f.7 to remove the requirement to perform the hot restart test
within 5 minutes of completing the 24-hour endurance test and place
that requirement in a separate TS.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
The proposed revision does not involve a significant hazards
consideration because operation of Callaway Plant with this change
would not:
(1) Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The proposed revision to the T/S will not adversely impact plant
safety since the requirement to perform the hot restart test will
still be implemented via a separate surveillance requirement that
demonstrates the hot restart functional capability of the diesel
generators.
(2) Create the possibility of a new or different kind of
accident from any previously evaluated.
There are no design changes being made that would create a new
type of accident or malfunction and the method and manner of plant
operation remain unchanged. The performance capability of the
emergency diesel generators will not be affected. The verification
of the hot restart capability of the diesel generators will still be
performed, only the timing of the performance will be changed to
give plant operators added flexibility and prevent critical path
complications during outages.
(3) Involve a significant reduction in a margin of safety.
There are no changes being made to the safety limits or safety
system settings that would adversely impact plant safety. The diesel
generators will still perform their intended safety function
following a loss of offsite power, to achieve and maintain the plant
in a safe shutdown condition.
Based on the above discussions, it has been determined that the
requested Technical Specification change does not involve a
significant increase in the probability or consequences of an
accident or create the possibility of a new or different kind of
accident or condition over previous evaluations; or involve a
significant reduction in a margin of safety. Therefore, the
requested license amendment does not involve a significant hazards
consideration.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Callaway County Public
Library, 710 Court Street, Fulton, Missouri 65251.
Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts
& Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Project Director: Leif J. Norrholm.
Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont
Yankee Nuclear Power Station, Vernon, Vermont
Date of amendment request: December 14, 1994.
Description of amendment request: The proposed amendment would
revise instrument identification for low reactor pressure instrument
trip cards in emergency core cooling system (ECCS) actuation to reflect
a design change to be installed during the 1995 refueling outage.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change to the identification numbers for certain
reactor pressure instrumentation as included in the Technical
Specifications for ECCS Actuation Instrumentation is only necessary
because the specific identification numbers (Tag Nos.) have been
listed in the [***]. This is considered an administrative type
change. Acceptable measurement of Low Reactor Pressure is still
assured. All automatic control or trip functions will continue to be
provided.
The proposed change does not result in any function or setpoint
change. The hardware changes which have resulted in a need to change
the Technical Specifications have removed instrumentation no longer
required to be installed in the circuitry for measuring ECCS Low
Reactor Pressure. The existing logic for Low Reactor Pressure will
remain the same. The only change applicable to implementation of the
design modification is the use of different trip cards to provide
the trip function for ECCS Low Reactor Pressure.
The requested change to ECCS Actuation Instrumentation Tables
does not impact any FSAR [Final Safety Analysis Report] safety
analysis involving the ECCS or Protection Systems. These measurement
functions are not contributors to the initiation of accidents.
The change in instrument Tag Nos. on Tables 3.2.1 and 4.2.1 will
have no affect on any safety limit setting or plant system operation
and, therefore, does not modify or add any initiating parameters
that would significantly increase the probability or consequences of
any previously analyzed accident.
The administrative change to correct a typographical error on
Table 4.2.1 will have no affect on plant hardware, plant design,
safety limit setting or plant system operation and, therefore, does
not modify or add any initiating parameters that would significantly
increase the probability or consequences of any previously analyzed
accident.
Therefore, it is concluded that there is not a significant
increase in the probability or consequence of an accident previously
evaluated.
2. The proposal to change instrument Tag Nos. does not result in
any function changes or changes to Technical Specification
requirements pertaining to these functions.
The proposed change does not involve any change in Technical
Specification trip setpoints, plant operation, redundancy,
protective function or design basis of the plant. There is no impact
on any existing safety analysis or safety design limits. Low Reactor
Pressure instrumentation functions do not initiate nuclear system
parameter variations which are considered potential initiating
causes of threats to the fuel and the nuclear system process barrier
or that would create any new or different kind of accident.
As discussed above, the proposed administrative change only
corrects a typographical error concerning equipment identification
numbers. This change does not affect any equipment and it does not
involve any potential initiating events that would create any new or
different kind of accident.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. The proposal to change the identification numbers for certain
reactor pressure instrumentation as included in the Technical
Specifications for ECCS Actuation Instrumentation does not affect
any existing safety margins. The change by itself is administrative.
The hardware changes which have resulted in a need to change the
Technical Specifications have been reviewed per 10 CFR 50.59(a)(2)
and determined to not constitute an unreviewed safety question.
The change in Tag Nos. or the change in the instrumentation used
to measure low [[Page 6316]] reactor pressure does not preclude the
ability of the Core Spray (CS) or Low Pressure Coolant Injection
(LPCI) Systems to perform their safety function to mitigate the
consequences of accidents or of any other safety system to
accomplish its safety functions. Proper post-accident ECCS
functioning will still be provided by safety class instruments used
to measure reactor pressure.
The change to instrument Tag Nos. as listed in the Technical
Specifications has no affect on the bases of Protective
Instrumentation which is to operate to initiate required system
protective actions. The changes to be implemented which have
resulted in a need to change the Technical Specifications will
actually improve the accuracy of reactor pressure measuring loops.
[***]
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Brooks Memorial Library, 224
Main Street, Brattleboro, Vermont 05301.
Attorney for licensee: John A. Ritsher, Esquire, Ropes and Gray,
One International Place, Boston, Massachusetts 02110-2624.
NRC Project Director: Walter R. Butler.
Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point
Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two Creeks,
Manitowoc County, Wisconsin
Date of amendment request: December 22, 1994.
Description of amendment request: The proposed amendment would
modify Point Beach Nuclear Plant Technical Specification (TS) Section
15.3.3, ``Emergency Core Cooling System, Auxiliary Cooling Systems, Air
Recirculation Fan Coolers, and Containment Spray,'' TS Section 15.3.4,
``Steam and Power Conversion System,'' TS Section 15.3.5,
``Instrumentation System,'' TS Section 15.3.7, ``Auxiliary Electrical
Systems,'' TS Section 15.3.14, ``Fire Protection System,'' and TS
Section 15.4.1, ``Operation Safety Review.'' The modifications would
delete obsolete TSs, would provide spring 1995 outage-specific TSs as
part of the ongoing diesel upgrade project, would update several TSs to
be consistent with the upgrade project design changes, and would change
one monthly testing requirement. In addition, the bases for Section TS
15.3.7 would be modified to be consistent with the proposed TS changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
In accordance with the requirements of 10 CFR 50.91(a),
Wisconsin Electric Power Company (Licensee) has evaluated the
proposed changes against the standards of 10 CFR 50.92 and has
determined that the operation of Point Beach Nuclear Plant, Units 1
and 2, in accordance with the proposed amendments [sic] does not
present a significant hazards consideration. The analysis of the
requirements of 10 CFR 50.92 and the basis for this conclusion are
as follows:
1. Operation of the facility under the proposed Technical
Specifications will not create a significant increase in the
probability or consequences of an accident previously evaluated.
The probabilities of accidents previously evaluated are based on
the probability of initiating events for these accidents. Initiating
events for accidents previously evaluated for Point Beach include:
control rod withdrawal and drop, CVCS malfunction (Boron Dilution),
startup of an inactive reactor coolant loop, reduction in feedwater
enthalpy, excessive load increase, losses of reactor coolant flow,
loss of external electrical load, loss of normal feedwater, loss of
all AC power to the auxiliaries, turbine overspeed, fuel handling
accidents, accidental releases of waste liquid or gas, steam
generator tube rupture, steam pipe rupture, control rod ejection,
and primary coolant system ruptures.
This license amendment request proposes to remove the
specifications associated with the 4160 volt safeguards bus tie, add
and modify specifications associated with the degraded and loss of
voltage protection functions, and remove specifications and
surveillance exceptions that are obsolete. The modifications being
performed and the changes proposed by this license amendment request
have been reviewed and we conclude that these changes do not
increase the probability of any initiating event for accidents
previously analyzed for Point Beach Nuclear Plant.
The consequences of the accidents previously evaluated in the
PBNP FSAR are determined by the results of analyses that are based
on initial conditions of the plant, the type of accident, transient
response of the plant, and the operation and failure of equipment
and systems. The changes proposed in this license amendment request
provide appropriate limiting conditions for operation, action
statements, allowable outage times, surveillances and bases for the
Point Beach Nuclear Plant Technical Specifications.
The proposed specification that allows a Train A service water
pump powered from the alternate shutdown system to be considered
operable under the provisions of Technical Specification 15.3.0.c is
appropriate to maintain operability of the service water system for
the continued safe operation of Unit 2 under the applicable standby
emergency power limiting condition for operation.
The modifications that are being performed have been designed
and will be installed in accordance with the applicable design and
installation requirements for Point Beach Nuclear Plant.
Therefore, this proposed license amendment does not affect the
consequences of any accident previously evaluated in the Point Beach
Nuclear Plant FSAR because the factors that are used to determine
the consequences of accidents are not being changed.
2. Operation of this facility under the proposed Technical
Specifications change will not create the possibility of a new or
different kind of accident from any accident previously evaluated.
New or different kinds of accidents can only be created by new
or different accident initiators or sequences. New and different
types of accidents (different from those that were originally
analyzed for Point Beach) have been evaluated and incorporated into
the licensing basis for Point Beach Nuclear Plant. Examples of
different accidents that have been incorporated into the Point Beach
Licensing basis include anticipated transients without scram and
station blackout.
The modifications being performed and the changes proposed by
this license amendment request have been reviewed and we conclude
that these changes do not create any new or different accident
initiators or sequences. Therefore, these modifications and proposed
Technical Specification changes do not create the possibility of an
accident of a different type than any previously evaluated in the
Point Beach FSAR.
3. Operation of this facility under the proposed Technical
Specifications change will not create a significant reduction in a
margin of safety.
The margins of safety for Point Beach are based on the design
and operation of the reactor and containment and the safety systems
that provide their protection. The modifications that are being
performed have been designed and will be installed in accordance
with the applicable design and installation requirements for Point
Beach Nuclear Plant.
The modification to change the loss of voltage protection
function from 1-out-of-2 logic on each bus to 2-out-of-3 logic on
each bus is an improvement over the original design, because with
the new design an inadvertent trip of a single channel will not
cause the protection actions. Also, when any single channel is taken
out-of-service for testing, maintenance, or calibration it can be
placed in the trip condition to allow actuation of the protection
function by the trip of either of the remaining operable channels.
The Technical Specification change to allow an operating pump
powered from alternate shutdown to be considered operable is
justified because the pump is able to perform its safety function
powered from the alternate shutdown power source. The alternate
shutdown system is powered via offsite power or from the onsite gas
turbine generator and is being considered a normal power supply for
the service water pump.
The alternate shutdown system was installed to provide an
alternate means of [[Page 6317]] providing power to service water
pumps, component cooling water pumps, and residual heat removal
pumps for certain 10 CFR 50 Appendix R fire scenarios in which the
normal power supplies for this equipment become inoperable. As such,
the alternate shutdown system is a qualified alternate source of
power for the service water pump.
Therefore, the margins of safety for Point Beach are not being
reduced because the design and operation of the reactor and
containment are not being changed and the safety systems that
provide their protection that are being changed are being modified
in accordance with the applicable design and installation
requirements for the Point Beach Nuclear Plant.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Joseph P. Mann Library, 1516
Sixteenth Street, Two Rivers, Wisconsin 54241.
Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts,
and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Project Director: Leif J. Norrholm.
Previously Published Notices of Consideration of Issuance of Amendments
to Facility Operating Licenses, Proposed no Significant Hazards
Consideration Determination, and Opportunity for a Hearing
The following notices were previously published as separate
individual notices. The notice content was the same as above. They were
published as individual notices either because time did not allow the
Commission to wait for this biweekly notice or because the action
involved exigent circumstances. They are repeated here because the
biweekly notice lists all amendments issued or proposed to be issued
involving no significant hazards consideration.
For details, see the individual notice in the Federal Register on
the day and page cited. This notice does not extend the notice period
of the original notice.
Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit Nos.
1, 2, and 3, Maricopa County, Arizona
Date of application for amendments: October 31, 1994, supplemented
by letter dated December 28, 1994.
Brief description of amendment requests: The proposed amendments
would change the refueling machine overload cutoff limit from less than
or equal to 1556 pounds to less than or equal to 1600 pounds. The
change is a consequence of the fuel assembly weight increase which
resulted from design and fabrication improvements.
Date of individual notice in Federal Register: January 6, 1995 (60
FR 2160).
Expiration date of individual notice: February 6, 1995.
Local Public Document Room location: Phoenix Public Library, 12
East McDowell Road, Phoenix, Arizona 85004.
Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit
No. 1, Pope County, Arkansas
Date of amendment request: August 30, 1994.
Description of amendment request: The proposed amendment revises
technical specifications to address the installation of two battery
chargers on each vital 125 vdc power train in lieu of the ``swing''
battery charger that is currently used.
Date of individual notice in the Federal Register: January 17, 1995
(60 FR 3439).
Expiration date of individual notice: February 16, 1995.
Local Public Document Room location: Tomlinson Library, Arkansas
Tech University, Russellville, Arkansas 728011.
Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388
Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County,
Pennsylvania
Date of amendment request: October 21, 1994.
Brief description of amendment request: The proposed amendment
would add the Special Test Exception 3/4.10.6, ``Inservice Leak and
Hydrostatic Testing,'' that allows the performance of pressure testing
at reactor coolant temperature up to 212 deg.F while remaining in
OPERATIONAL CONDITION 4. This special test exception would also require
that certain OPERATIONAL CONDITION 3 Specifications for Secondary
Containment Isolation, Secondary Containment Integrity and Standby Gas
Treatment System operability be met. This change would also revise the
Index, Table 1.2, ``OPERATIONAL CONDITIONS,'' and the Bases to
incorporate the reference to the proposed special test exception.
Date of publication of individual notice in Federal Register:
December 22, 1994 (59 FR 66057).
Expiration date of individual notice: January 23, 1995.
Local Public Document Room location: Osterhout Free Library,
Reference Department, 71 South Franklin Street, Wilkes-Barre,
Pennsylvania 18701.
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of application for amendment: December 8, 1994.
Brief description of amendment: The proposed amendment would revise
Section 4.4 of the Indian Point 3 Technical Specifications.
Specifically, TS 4.4.E.1 would be revised to allow a one-time extension
to the 30-month interval requirement for leak rate testing of Residual
Heat Removal (RHR) containment isolation valves AC-732, AC-741, AC-MOV-
743, AC-MOV-744, and AC-MOV-1870. This one-time extension for leak rate
testing of the RHR valves would be deferred until prior to return to
power following the current outage, which is defined as prior to
Tavg exceeding 350 deg.F.
Date of publication of individual notice in Federal Register:
December 13, 1994 (59 FR 64224).
Expiration date of individual notice: January 12, 1995.
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10610.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of application for amendments: December 16, 1994.
Brief description of amendments: This amendment would revise
Technical Specifications regarding diesel generator surveillance
requirements.
Date of publication of individual notice in the Federal Register:
December 22, 1994 (59 FR 67350).
Expiration date of individual notice: January 23, 1995.
Local Public Document Room location: Chattanooga-Hamilton County
Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of application for amendments: January 3, 1995.
Brief description of amendments: The amendments add a permissive
statement to Surveillance Requirement 4.9.7.1 that [[Page 6318]] will
allow the auxiliary building bridge crane interlocks and physical stops
to be defeated during implementation of the spent fuel pool storage
capacity increase modification.
Date of publication of individual notice in the Federal Register:
January 9, 1995 (60 FR 2404).
Expiration date of individual notice: January 24, 1995.
Local Public Document Room location: Chattanooga-Hamilton County
Library, 1101 Broad Street, Chattanooga, Tennesee 37402.
Notice of Insurance of Amendments to Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR Chapter I, which are set
forth in the license amendment.
Notice of Consideration of Issuance of Amendment to Facility
Operating License, Proposed No Significant Hazards Consideration
Determination, and Opportunity for A Hearing in connection with these
actions was published in the Federal Register as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.12(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items are available for public inspection at
the Commission's Public Document Room, the Gelman Building, 2120 L
Street, NW., Washington, DC, and at the local public document rooms for
the particular facilities involved.
Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318,
Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County,
Maryland
Date of application for amendments: September 23, 1994.
Brief description of amendments: The amendments revise the Unit 2
Shutdown AC Power Sources TSs to permit a one-time increase the allowed
outage time (AOT) from 7 to 14 days for the dedicated Class IE
emergency power system and the Unit 1 control room emergency
ventilation system TSs to permit a one-time increase the AOT from 7 to
30 days. These one-time extensions are necessary to support
modifications scheduled to be implemented during the upcoming 1995 Unit
2 refueling outage.
Date of issuance: January 11, 1995.
Effective date: As of the date of issuance to be implemented during
the 1995 Unit 2 refueling outage.
Amendment Nos.: Unit 1-202 and Unit 2-180.
Facility Operating License Nos. DPR-53 and DPR-69: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: October 26, 1994 (59 FR
53835).
The Commission's related evaluation of these amendments is
contained in a Safety Evaluation dated January 11, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Calvert County Library, Prince
Frederick, Maryland 20678.
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North
Carolina
Date of application for amendment: May 15, 1993, as supplemented
February 17, 1994, February 25, 1994, and November 23, 1994.
Brief description of amendment: The amendment deletes Section
2.C.(8) of the Facility Operating License NPF-63, and deletes
Attachment 1 to the License, in response to your request dated May 15,
1993, as supplemented February 17, 1994, February 25, 1994, and
November 23, 1994
Date of issuance: January 12, 1995.
Effective date: January 12, 1995.
Amendment No. 53.
Facility Operating License No. NPF-63. Amendment revises the
Technical Specifications.
Date of initial notice in Federal Register: June 9, 1993 (58 FR
32378).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 12, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Cameron Village Regional
Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. STN
50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will
County, Illinois
Date of application for amendments: June 3, 1994.
Brief description of amendments: The amendments revise Byron and
Braidwood technical specifications (TSs) to reflect a primary-to-
secondary leakage rate of 150 gallons per day through any one steam
generator and to reflect an inservice inspection of a minimum of 20
percent of a random sample of the sleeves at the end-of-cycle. The
amendment also adds a condition to the licenses to conduct additional
corrosion testing to establish the design life for the sleeved tubes in
the presence of a crevice. The revised TSs are more conservative than
the previous TSs and were requested in order to increase the confidence
in the ability of sleeves to maintain primary-to-secondary integrity.
Date of issuance: January 6, 1995.
Effective date: January 6, 1995.
Amendment Nos.: 67, 67, 57, and 57.
Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77:
The amendments revised the operating licenses and TSs.
Date of initial notice in Federal Register: October 12, 1994 (59 FR
51613). The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 6, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: For Byron, the Byron Public
Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for
Braidwood, the Wilmington Township Public Library, 201 S. Kankakee
Street, Wilmington, Illinois 60481. [[Page 6319]]
Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. STN
50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will
County, Illinois
Date of application for amendments: November 7, 1994, as
supplemented December 16, 1994.
Brief description of amendments: The amendments approve the use and
storage of fuel with an enrichment not to exceed a nominal 5.0 weight
percent U-235 in the spent fuel racks.
Date of issuance: January 20, 1995.
Effective date: January 20, 1995.
Amendment Nos.: 68, 68, 58, and 58.
Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77:
The amendments revised the Technical Specifications.
Date of initial notice in Federal Register: December 7, 1994 (59 FR
63115). The December 16, 1994, submittal provided additional clarifying
information that did not change the initial proposed no significant
hazards consideration determination. The Commission's related
evaluation of the amendments is contained in an Environmental
Assessment dated January 13, 1995, and in a Safety Evaluation dated
January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: For Byron, the Byron Public
Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for
Braidwood, the Wilmington Township Public Library, 201 S. Kankakee
Street, Wilmington, Illinois 60481.
Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of application for amendments: January 10, 1994, as
supplemented September 15, 1994, January 5 and 10, 1995.
Brief description of amendments: The amendments revise Technical
Specification (TS) Table 2.2-1 and TS 4.2.5 to allow a change in the
method for measuring reactor coolant system (RCS) flow rate from the
calorimetric heat balance method to a method based on a calibration of
the RCS cold leg elbow differential pressure taps.
Date of issuance: January 12, 1995.
Effective date: To be implemented within 30 days from the date of
issuance.
Amendment Nos.: 153 and 135.
Facility Operating License Nos. NPF-9 and NPF-17: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: February 16, 1994 (59
FR 7688). The September 15, 1994, January 5 and 10, 1995, letters
provided clarifying information that did not change the scope of the
January 10, 1994, application, the Federal Register Notice or the
initial proposed no significant hazards consideration determination.
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 12, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Atkins Library, University of
North Carolina, Charlotte (UNCC Station), North Carolina 28223
Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389,
St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
Date of application for amendments: November 2, 1994.
Brief description of amendments: These amendments clarify the
actions required in the event of inoperable equipment associated with
containment depressurization and cooling systems, and provide
consistency between Unit 1 and Unit 2 requirements.
Date of Issuance: January 18, 1995.
Effective Date: January 18, 1995.
Amendment Nos.: 131 and 70.
Facility Operating License Nos. DPR-67 and NPF-16: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: December 7, 1994 (59 FR
63122).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 18, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Indian River Junior College
Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey
Point Plant Units 3 and 4, Dade County, Florida
Date of application for amendments: April 19, 1994.
Brief description of amendments: These amendments consist of
changes to the Technical Specifications relating to surveillance
requirements for inservice inspection and testing programs.
Date of issuance: January 11, 1995.
Effective date: January 11, 1995.
Amendment Nos. 171 and 165.
Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: May 25, 1994 (59 FR
27054).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 11, 1995.
No significant hazards consideration comments received: No
Local Public Document Room location: Florida International
University, University Park, Miami, Florida 33199.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket No. 50-424,
Vogtle Electric Generating Plant, Unit 1, Burke County, Georgia
Date of application for amendment: August 16, 1994.
Brief description of amendment: The amendment eliminated License
Condition 2.C.(6) and the associated Attachment 1 of the license.
License Condition 2.C.(6) referenced Attachment 1 which listed special
diesel generator maintenance and surveillance requirements.
Date of issuance: January 20, 1995.
Effective date: To be implemented within 30 days from the date of
issuance.
Amendment No.: 81.
Facility Operating License Nos. NPF-68: Amendment revised the
Facility Operating License.
Date of initial notice in Federal Register: September 6, 1994 (59
FR 46071).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Burke County Library, 412
Fourth Street, Waynesboro, Georgia 30830.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of application for amendments: March 31, 1994.
Brief description of amendments: The changes revised TS Table 3.7-1
by lowering the maximum allowable power range neutron flux high
setpoint when one or more main steam safety valves (MSSVs) are
inoperable. The changes also revised the Bases for TS 3/4.7.1.1
[[Page 6320]] to include the Westinghouse algorithm for determining the
new setpoint values.
Date of issuance: January 20, 1995.
Effective date: To be implemented within 30 days from date of
issuance.
Amendment Nos.: 82 and 60.
Facility Operating License Nos. NPF-68 and NPF-81: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: July 20, 1994 (59 FR
37071).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Burke County Library, 412
Fourth Street, Waynesboro, Georgia 30830.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of application for amendments: May 20, 1994.
Brief description of amendments: The amendments relocate the heat
flux hot channel factor, FQ(Z), penalty of 2 percent in
specification 4.2.2.2.f to the cycle-specific Core Operating Limits
Report (COLR) to allow for burnup-dependent values of the penalty in
excess of 2 percent. This amendment also revises the reference in
specification 6.8.1.6 to the Westinghouse FQ(Z) surveillance
methodology in order to reflect Revision 1 of WCAP-10216-P,
``Relaxation of Constant Axial Offset Control--FQ Surveillance
Technical Specification,'' approved by the NRC on November 26, 1993.
Date of issuance: January 11, 1995.
Effective date: To be implemented within 30 days from the date of
issuance.
Amendment Nos.: 79 and 58.
Facility Operating License Nos. NPF-68 and NPF-81: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: July 20, 1994 (59 FR
37072). The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 11, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Burke County Library, 412
Fourth Street, Waynesboro, Georgia 30830.
Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric
Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and
50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of application for amendments: August 16, 1994.
Brief description of amendments: The amendments change Technical
Specification 3/4.7.1.1 and its Bases regarding the setpoint tolerance
for the main steam safety valves.
Date of issuance: January 12, 1995.
Effective date: To be implemented within 30 days from the date of
issuance.
Amendment Nos.: 80 and 59.
Facility Operating License Nos. NPF-68 and NPF-81: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: September 14, 1994 (59
FR 47168).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 12, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Burke County Library, 412
Fourth Street, Waynesboro, Georgia 30830.
IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center,
Linn County, Iowa
Date of application for amendment: July 29, 1994.
Brief description of amendment: The proposed amendment would revise
the Technical Specifications by deleting reference to written relief
from ASME Code requirements. The revised Technical Specifications refer
to the applicable provision of NRC regulations concerning the ASME
Code.
Date of issuance: January 6, 1995.
Effective date: January 6, 1995, to be implemented within 120 days.
Amendment No.: 206.
Facility Operating License No. DPR-49. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: August 31, 1994 (59 FR
45026).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 6, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Cedar Rapids Public Library,
500 First Street, SE., Cedar Rapids, Iowa 52401.
Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee
Atomic Power Station, Lincoln County, Maine
Date of application for amendment: March 15, 1994, as supplemented
October 20, 1994.
Brief description of amendment: This amendment allows the use of
integral fuel burnable absorbers as a method of controlling core excess
reactivity and maintaining core power distribution within acceptable
peaking limitations.
Date of issuance: January 17, 1995
Effective date: January 17, 1995.
Amendment No.: 145.
Facility Operating License No. DPR-36: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: April 28, 1994 (59 FR
22010).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 17, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Wiscasset Public Library, High
Street, P.O. Box 367, Wiscasset, Maine 04578.
Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point
Nuclear Station, Unit 2, Oswego County, New York
Date of application for amendment: October 5, 1994.
Brief description of amendment: The amendment revises the
applicability requirements of Technical Specification (TS) 3.7.3 to
require operability of the Control Room Outdoor Air Special Filter
Train System in Operational Conditions 1, 2, 3 and ** rather than in
all Operational Conditions and **. The applicability requirements for
Action Statement b. of TS 3.7.3 and for the Radiation Monitoring
Instrumentation required operable by TS Tables 3.3.7.1-1 and 4.3.7.1-1
are being changed in a similar manner. The amendment also adds a
notation to Action Statement b.1. of TS 3.7.3 stating that the
provisions of TS 3.0.4 are not applicable for entry into Operational
Condition ** when one filter train is inoperable provided an operable
filter train is in operation in the emergency pressurization mode of
operation.
Date of issuance: January 18, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 60.
Facility Operating License No. NPF-69: Amendment revises the
Technical Specifications. [[Page 6321]]
Date of initial notice in Federal Register: November 9, 1994 (59 FR
55874).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 18, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Reference and Documents
Department, Penfield Library, State University of New York, Oswego, New
York 13126.
Northeast Nuclear Energy Company, Docket No. 50-245, Millstone Nuclear
Power Station, Unit 1, New London County, Connecticut
Date of application for amendment: October 4, 1994.
Brief description of amendment: The amendment relocates the primary
containment isolation valve list from Technical Specification (TS)
Section 3.7.D to the Millstone Unit 1 Technical Requirements Manual.
This change is in accordance with the guidance of Generic Letter 91-08.
The amendment also makes administrative and editorial changes to TS
Sections 3.7.D and 4.7.D and makes changes to the associated bases.
Date of issuance: January 10, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 78.
Facility Operating License No. DPR-21. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: November 23, 1994 (59
FR 60383)
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 10, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Learning Resource Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Northeast Nuclear Energy Company, Docket No. 50-245, Millstone Nuclear
Power Station, Unit 1, New London County, Connecticut
Date of application for amendment: October 14, 1994.
Brief description of amendment: The amendment clarifies the low
pressure coolant injection requirements as required by Technical
Specification 4.5.A.2.
Date of issuance: January 9, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 77.
Facility Operating License No. DPR-21. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: December 7, 1994 (59 FR
63125).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 9, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Learning Resource Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone
Nuclear Power Station, Unit No. 3, New London County, Connecticut
Date of application for amendment: September 9, 1994, with
clarifying information provided by letter dated October 5, 1994.
Brief description of amendment: The amendment revises the Technical
Specifications to modify surveillance requirements by increasing the
acceptance criterion for the closure of the main steam isolation valves
from 5 seconds to 10 seconds.
Date of issuance: January 10, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 101.
Facility Operating License No. NPF-49. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: September 19, 1994 (59
FR 47960). The October 5, 1994, letter provided clarifying information
that did not change the initial proposed no significant hazards
consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated Janaury 10, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Learning Resources Center,
Three Rivers Community-Technical College, Thames Valley Campus, 574 New
London Turnpike, Norwich, CT 06360.
Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County,
Minnesota
Date of application for amendments: October 17, 1994, as
supplemented October 27, 1994.
Brief description of amendments: The amendments revise the Prairie
Island Nuclear Generating Plant Technical Specifications to change the
submittal frequency of the Radioactive Effluent Release Report from
semiannual to annual in accordance with 10 CFR Part 50.36a.
Date of issuance: January 11, 1995.
Effective date: January 11, 1995, with full implementation within
30 days.
Amendment Nos.: 114 and 107.
Facility Operating License Nos. DPR-42 and DPR-60. Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: December 7, 1994 (59 FR
63125) The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 11, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401.
Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388
Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County,
Pennsylvania
Date of application for amendments: July 27, 1994.
Brief description of amendments: These amendments revise the
Technical Specifications (TS) definition of ``Core Alteration'' to
conform to the definition approved by the staff for the current boiling
water reactor (BWR) improved TS in NUREG-1433, ``Standard Technical
Specifications, General Electric Plants, BWR/4.''
Date of issuance: January 3, 1995.
Effective date: January 3, 1995.
Amendment Nos.: 138 and 108.
Facility Operating License Nos. NPF-14 and NPF-22. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: September 14, 1994 (59
FR 47177).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 3, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Osterhout Free Library,
[[Page 6322]] Reference Department, 71 South Franklin Street, Wilkes-
Barre, Pennsylvania 18701.
Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388
Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County,
Pennsylvania
Date of application for amendments: August 22, 1994.
Brief description of amendments: These amendments change Technical
Specifications 3/4.1.3 to: (1) Extend the scram discharge volume (SDV)
vent or drain valve restoration time from the current time period of 24
hours to 7 days; (2) permit the SDV vent and drain valves operability
check to be performed at shutdown conditions instead of at-least-once-
per-18-months; and (3) delete the SDV float switch response
surveillance requirement.
Date of issuance: January 9, 1995.
Effective date: January 9, 1995.
Amendment Nos.: 139 and 109.
Facility Operating License Nos. NPF-14 and NPF-22. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: September 28, 1994 (59
FR 49433).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 9, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Osterhout Free Library,
Reference Department, 71 South Franklin Street, Wilkes-Barre,
Pennsylvania 18701.
Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388
Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County,
Pennsylvania
Date of application for amendments: September 26, 1994.
Brief description of amendments: The amendments change the
Technical Specifications for each of the units to remove the
requirement for the average power range monitors (APRMs) to be operable
while the plant is in Operational Condition 5, refueling status.
However, the amendment does not change the requirement for the APRMs to
be operable when the reactor mode switch is in Startup during a
shutdown margin demonstration.
Date of issuance: January 9, 1995.
Effective date: January 9, 1995.
Amendment Nos.: 140 and 110.
Facility Operating License Nos. NPF-14 and NPF-22. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: November 9, 1994 (59 FR
55880).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 9, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Osterhout Free Library,
Reference Department, 71 South Franklin Street, Wilkes-Barre,
Pennsylvania 18701.
Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick
Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
Date of application for amendments: August 25, 1993, as
supplemented by letter dated August 4, 1994.
Brief description of amendments: These amendments modify Technical
Specification (TS) Section 3.3.7.8.2 and associated Bases 3/4.3.7.8
regarding the Main Control Room (MCR) toxic gas detection system. The
TS change reflects the implementation of a modification designed to
eliminate spurious high toxic gas concentration alarms received by the
MCR.
Date of issuance: January 19, 1995.
Effective date: January 19, 1995.
Amendment Nos. 84 and 45.
Facility Operating License Nos. NPF-39 and NPF-85. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: September 29, 1993 (58
FR 50971).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 19, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, Pennsylvania 19464.
Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick
Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
Date of application for amendments: July 20, 1994, as supplemented
September 23, 1994.
Brief description of amendments: The amendments would raise the
Steam Leakage Detection system set-points that isolate the High
Pressure Coolant Injection System (HPCI) and Reactor Core Isolation
Cooling (RCIC) system equipment on high equipment room temperature and
high delta temperature. The amendments are supported by a Limerick
Generating Station modification to increase the environmental
qualifications limits of the HPCI and RCIC systems to allow the systems
to remain operable when equipment room cooling is unavailable.
Date of issuance: January 20, 1995.
Effective date: January 20, 1995.
Amendment Nos. 85 and 46.
Facility Operating License Nos. NPF-39 and NPF-85. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: September 14, 1994 (59
FR 47178).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, Pennsylvania 19464.
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of application for amendment: April 18,1994, as supplemented
October 25, 1994.
Brief description of amendment: The amendment revises TS Section
3.14 (Fire Protection and Detection Systems--Limiting Conditions for
Operation), TS Section 4.12 (Fire Protection and Detection Systems--
Surveillances) and TS Section 6.0 (Administrative Controls) to relocate
the fire protection requirements from the TSs to the IP3 Operational
Specifications Manual. In addition, the amendment revised the IP3
Facility Operating License to include the NRC's standard fire
protection license condition. These changes were made in accordance
with the guidance provided in Generic Letter (GL) 86-10,
``Implementation of Fire Protection Requirements,'' and GL 88-12,
``Removal of Fire Protection Requirements from Technical
Specifications.''
Date of issuance: January 13, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 157.
Facility Operating License No. DPR-64: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: May 25, 1994 (59 FR
27065).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 13, 1995.
No significant hazards consideration comments received: No.
[[Page 6323]]
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10610.
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of application for amendment: December 8, 1994.
Brief description of amendment: The amendment revises TS section
4.4.E.1 to allow a one-time extension to the 30-month interval
requirement for leak rate testing of Residual Heat Removal containment
isolation valves AC-732, AC-741, AC-MOV-743, AC-MOV-744 and AC-MOV-
1870.
Date of issuance: January 13, 1995.
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 158.
Facility Operating License No. DPR-64: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: December 13, 1994 (59
FR 64223).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 13, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10610.
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of application for amendment: June 29, 1994, as supplemented
December 2, 1994.
Brief description of amendment: The amendment revised Technical
Specification (TS) Section 6.5, ``Review and Audit,'' and TS Section
6.8, ``Procedures,'' to establish a new review and approval process for
nuclear safety-related procedures and to modify membership requirements
for the Plant Operating Review Committee. The amendment also revised TS
Section 6.5 to delete review and audit responsibilities for the
Emergency and Security Plans consistent with Generic Letter 93-07,
``Modification of the Technical Specification Administrative Control
Requirements for Emergency and Security Plans.''
Date of issuance: January 17, 1995.
Effective date: As of the date of issuance to be implemented within
90 days.
Amendment No.: 159.
Facility Operating License No. DPR-64: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: July 20, 1994 (59 FR
37081).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 17, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10610.
Power Authority of the State of New York, Docket No. 50-333, James A.
FitzPatrick Nuclear Power Plant, Oswego County, New York
Date of application for amendment: June 17, 1994, as supplemented
December 2, 1994.
Brief description of amendment: The amendment revises Section 6.5,
``Review and Audit,'' and Section 6.8, ``Procedures,'' of the Technical
Specifications (TSs) to establish a new review and approval process for
nuclear safety-related procedures. The amendment also revises Section
6.5 to modify membership requirements for the Plant Operating Review
Committee and to delete review and audit responsibilities for the
Emergency and Security Plans from the TSs consistent with Generic
Letter 93-07, ``Modification of the Technical Specification
Administrative Control Requirements for Emergency and Security Plans.''
Date of issuance: January 18, 1995.
Effective date: As of the date of issuance to be implemented within
90 days.
Amendment No.: 222.
Facility Operating License No. DPR-59: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: July 20, 1994 (59 FR
37082).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 18, 1995.
No significant hazards consideration comments received: No
Local Public Document Room location: Reference and Documents
Department, Penfield Library, State University of New York, Oswego, New
York 13126.
The Cleveland Electric Illuminating Company, Centerior Service Company,
Duquesne Light Company, Ohio Edison Company, Pennsylvania Power
Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power
Plant, Unit No. 1, Lake County, Ohio
Date of application for amendment: September 19, 1994.
Brief description of amendment: The amendment revised the Technical
Specifications for the snubber visual inspection schedule.
Date of issuance: January 20, 1995.
Effective date: January 20, 1995 and to be implemented within 90
days.
Amendment No. 68.
Facility Operating License No. NPF-58. This amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: October 26, 1994 (59 FR
53843).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Perry Public Library, 3753
Main Street, Perry, Ohio 44081.
Toledo Edison Company, Centerior Service Company, and The Cleveland
Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear
Power Station, Unit No. 1, Ottawa County, Ohio
Date of application for amendment: May 1, 1992 as clarified by
facsimile transmission dated January 10, 1995.
Brief description of amendment: The amendment revises the LIMITING
CONDITIONS FOR OPERATION and SURVEILLANCE REQUIREMENTS for the
containment air locks, changes the exception for containment
penetration status verification to include the annulus, clarifies
containment air lock testing intervals, and clarifies the definition
and bases for containment integrity.
Date of issuance: January 17, 1995.
Effective date: Date of issuance and to be implemented within 90
days.
Amendment No. 194.
Facility Operating License No. NPF-3. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: September 2, 1992 (57
FR 40221).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 17, 1995. [[Page 6324]]
No significant hazards consideration comments received: No.
Local Public Document Room location: University of Toledo Library,
Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
Washington Public Power Supply System, Docket No. 50-397, Nuclear
Project No. 2, Benton County, Washington
Date of application for amendment: August 8, 1994.
Brief description of amendment: The amendment modifies the
Technical Specifications (TS) to delete the requirement to obtain prior
written relief from the Commission for inservice inspection (ISI) and
inservice testing (IST) of components conducts pursuant to 10 CFR
50.55a. The amendment also adds a definition for the word ``biennial.''
Date of issuance: January 5, 1995.
Effective date: January 5, 1995.
Amendment No.: 133.
Facility Operating License No. NPF-21: The amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: November 14, 1994 (59
FR 56558).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 5, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room location: Richland Public Library, 955
Northgate Street, Richland, Washington 99352.
Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point
Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, Manitowoc
County, Wisconsin
Date of application for amendments: November 23, 1993, as
supplemented January 10, 12, and 13, 1995.
Brief description of amendments: These amendments revise the
operating conditions and limiting conditions for operation for
containment systems, and revise corresponding definitions and tests. In
addition, the related bases are updated to ensure consistency and
clarity.
Date of issuance: January 18, 1995.
Effective date: January 18, 1995, to be implemented within 45 days.
Amendment Nos.: 160 and 164.
Facility Operating License Nos. DPR-24 and DPR-27. Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: January 19, 1994 (59 FR
2875).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated January 18, 1995.
The January 10, 12, and 13, 1995 submittals provided supplemental
information that did not change the initial proposed no significant
hazards consideration determination.
No significant hazards consideration comments received: No.
Local Public Document Room location: Joseph P. Mann Library, 1516
Sixteenth Street, Two Rivers, Wisconsin 54241.
Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek
Generating Station, Coffey County, Kansas
Date of amendment request: October 27, 1993.
Brief description of amendment: The amendment changes Note 5 of
Technical Specification Table 4.3-1 to reflect the use of integral bias
curves, rather than detector plateau curves, to calibrate the source
range instrumentation.
Date of issuance: January 9, 1995.
Effective date: January 9, 1995, to be implemented within 30 days.
Amendment No.: 83.
Facility Operating License No. NPF-42. The amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: November 24, 1993 (58
FR 62159). The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated January 9, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room locations: Emporia State University,
William Allen White Library, 1200 Commercial Street, Emporia, Kansas
66801 and Washburn University School of Law Library, Topeka, Kansas
66621.
Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek
Generating Station, Coffey County, Kansas
Date of amendment request: October 21, 1994, as supplemented by
letters dated October 27, 1994 and December 2, 1994.
Brief description of amendment: This amendment revises Technical
Specification (TS) Surveillance Requirements 4.7.1.2.1.c.2, operability
testing of the auxiliary feedwater (AFW) pump auto start feature, and
4.3.2.2, engineered safety features (ESF) time response testing of the
AFW pumps to exempt the testing of the turbine-driven AFW pump from the
provisions of TS 4.0.4 for entry into Mode 3. In addition, TS
Surveillance Requirement 4.7.1.2.1.c is revised to delete the
requirement that the 18 month AFW surveillance be performed during
shutdown.
Date of issuance: January 20, 1995.
Effective date: January 20, 1995, to be implemented within 30 days.
Amendment No.: 84.
Facility Operating License No. NPF-42. The amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: November 23, 1994 (59
FR 60389) The December 2, 1994, supplemental letter provided clarifying
information and did not change the initial no significant hazards
consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated January 20, 1995.
No significant hazards consideration comments received: No.
Local Public Document Room locations: Emporia State University,
William Allen White Library, 1200 Commercial Street, Emporia, Kansas
66801 and Washburn University School of Law Library, Topeka, Kansas
66621.
Dated at Rockville, Maryland, this 25th day of January 1995.
For the Nuclear Regulatory Commission.
Jack W. Roe,
Director, Division of Reactor Projects--III/IV, Office of Nuclear
Reactor Regulation.
[FR Doc. 95-2350 Filed 1-31-95; 8:45 am]
BILLING CODE 7590-01-P